Gear-up landing Accident Aero Commander 200D N49J,
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ASN Wikibase Occurrence # 202073
 
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Date:Saturday 13 March 1999
Time:11:45 LT
Type:Silhouette image of generic M200 model; specific model in this crash may look slightly different    
Aero Commander 200D
Owner/operator:Jerry D. Weathers
Registration: N49J
MSN: 352
Total airframe hrs:3500 hours
Engine model:Continental IO-520-A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Evanston, WY -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:(KEVW)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was conducting a test flight after recent maintenance work had been performed on the engine. A thorough preflight was performed, and no water was found in the fuel. The pilot completed an extended run-up at all throttle positions, including a mock takeoff to a full stop. After an uneventful departure, the nose landing gear light failed to indicate that it was in the up and locked position. The pilot climbed to 10,000 feet and attempted to recycle the landing gear, but was unsuccessful. He over flew the airport to have a ground observer verify the landing gear's position. According to the pilot, 'about that time the engine quit without warning... The engine sputtered a second, then stopped again, with the electric fuel pump [on].' He performed an emergency gear-up landing on the runway. A postaccident engine examination was performed by an FAA inspector, including an inspection of the electrically-driven fuel pump that had recently been replaced. Fuel was present in each of the fuel injector nozzles and no engine discrepancies were observed.

Probable Cause: A total loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN99LA056
Status: Investigation completed
Duration: 2 years 1 month
Download report: Final report

Sources:

NTSB DEN99LA056

History of this aircraft

Other occurrences involving this aircraft
18 January 2005 N49J Private Hatch, Utah sub

Location

Revision history:

Date/timeContributorUpdates
26-Nov-2017 10:55 ASN Update Bot Added
08-Apr-2024 08:46 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

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