ASN Wikibase Occurrence # 206282
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Date: | Friday 16 February 2018 |
Time: | 13:20 |
Type: | Thorp T-18 Tiger |
Owner/operator: | Private |
Registration: | N89ER |
MSN: | 1106 |
Year of manufacture: | 1978 |
Total airframe hrs: | 1634 hours |
Engine model: | Lycoming O-320-B3B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Vance Brand Airport (KLMO), Longmont, CO -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Longmont, CO (LMO) |
Destination airport: | Longmont, CO (LMO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The tailwheel-qualified private pilot was conducting his first flight in the T-18 airplane with a flight instructor. After several local flight maneuvers and about seven uneventful landings, he planned to execute a full-stop landing. During the landing roll, the airplane turned right as it decelerated. The pilot attempted to correct the turn with left rudder control and braking, but the airplane groundlooped, departed the runway surface, and nosed over, which resulted in damage to the left wing and vertical stabilizer. The pilot was unsure if he had applied any braking pressure during the landing before having directional control issues. The flight instructor did not recall the accident sequence due to his injuries. Postaccident examination of the airplane revealed no evidence of mechanical malfunctions or failures, except for a fractured rudder cable. Examination of the cable revealed an overstress separation, which was consistent with accident damage. Thus, the pilot likely failed to maintain directional control during the landing roll and the flight instructor did not take timely remedial action to maintain runway heading.
Probable Cause: The pilot’s failure to maintain directional control during the landing roll and the flight instructor’s delayed remedial action, which resulted in a groundloop and nose over.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA102 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N89ER
History of this aircraft
Other occurrences involving this aircraft Location
Media:
Revision history:
Date/time | Contributor | Updates |
17-Feb-2018 12:54 |
Iceman 29 |
Added |
17-Feb-2018 17:58 |
Aerossurance |
Updated [Location, Embed code] |
11-Nov-2019 17:42 |
ASN Update Bot |
Updated [Time, Departure airport, Destination airport, Source, Embed code, Narrative, Accident report, ] |
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