Accident Raytheon A36 Bonanza N207PC,
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ASN Wikibase Occurrence # 207038
 
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Date:Sunday 4 March 2018
Time:16:58 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Raytheon A36 Bonanza
Owner/operator:Systima Technologies INC
Registration: N207PC
MSN: E-3503
Year of manufacture:2003
Total airframe hrs:1069 hours
Engine model:Continental IO-550B39
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:King County, Enumclaw, WA -   United States of America
Phase: Landing
Nature:Private
Departure airport:Yuma MCAS/Yuma International Airport, AZ (YUM/KNYL)
Destination airport:Everett-Snohomish County Airport, WA (PAE/KPAE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was at cruise altitude en route on a cross-country flight from Arizona to Washington when he noted that the engine oil pressure indicated zero and the manifold pressure was near zero. He then heard ''¦a loud bang, as though the engine had thrown a rod.' The cabin filled with smoke and oil covered the windscreen, and the pilot conducted a forced landing into a stand of trees, during which the airplane sustained substantial damage.

Examination of the airframe revealed no anomalies that would have precluded normal operation. An examination of the engine revealed three holes in the crankcase, each consistent with an internal engine failure. All six cylinders remained attached to their respective cylinder bays; there was no indication of impact damage. The Nos. 2, 4 and 5 connecting rods had separated from the crankshaft. All rod bearings displayed lubrication distress consistent with oil starvation. The oil line B-nut attached to the turbocharger scavenge check valve was loose.

Based on the available information, it is likely that the loose oil line B-nut resulted in a gradual loss of oil during the long cross-country flight, which subsequently resulted in the separation of the connecting rods due to oil starvation and a total loss of engine power.

Probable Cause: A total loss of engine power due to oil starvation as a result of a loose oil line B-nut.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR18LA098
Status: Investigation completed
Duration: 3 years and 2 months
Download report: Final report

Sources:

NTSB WPR18LA098

https://flightaware.com/live/flight/N207PC

Location

Media:

Revision history:

Date/timeContributorUpdates
05-Mar-2018 03:09 Geno Added
05-Mar-2018 03:30 Geno Updated [Aircraft type, Registration, Cn, Operator, Destination airport, Source, Narrative]
05-Mar-2018 03:35 Iceman 29 Updated [Time, Aircraft type, Registration, Cn, Operator, Destination airport, Source, Embed code, Narrative]
05-Mar-2018 18:48 harro Updated [Aircraft type, Embed code]
06-Mar-2018 16:14 Iceman 29 Updated [Aircraft type, Registration, Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative]
01-Jan-2021 23:09 Geno Updated [Time, Aircraft type, Departure airport, Destination airport, Source]
09-Jul-2022 12:36 ASN Update Bot Updated [Time, Other fatalities, Source, Damage, Narrative, Category, Accident report]

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