Incident Piper PA-28R-180 VH-BOP,
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ASN Wikibase Occurrence # 210252
 
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Date:Monday 27 January 1997
Time:15:00
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-180
Owner/operator:
Registration: VH-BOP
MSN: 28R-31268
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Location:Wynyard, TAS -   Australia
Phase: Unknown
Nature:Private
Departure airport:YWYY
Destination airport:YMMB
Investigating agency: BASI
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the initial climb, the engine suffered a power loss. The pilot observed the manifold pressure decreasing so he selected alternate air, checked the mixture control was set to rich and checked the fuel pump was switched on. He changed the fuel selection from the left tank to the right tank, but the engine did not respond. By this time the aircraft was low over the water so the pilot transmitted a PAN call advising of the emergency and his intention to land on a beach. When the aircraft had descended to about three metres above the water and its speed had reduced to 60 knots, the pilot transmitted a MAYDAY call. Shortly afterwards the aircraft was stalled into the water at the mouth of the Inglis River. The impact forces damaged the fuselage which rapidly filled with water. The pilot and two passengers vacated the aircraft before it sank and were rescued by the crew of a nearby fishing boat. The investigation into the cause of the engine power loss was hindered because the aircraft was badly damaged during the accident and the subsequent recovery exercise. It was established that sufficient fuel was on board for the proposed flight and fuel was available to the fuel distributor, but the contents of the fuel filter assembly could not be determined. The engine was inspected and disassembled and relevant components were tested. It was found that the air duct hose fitted between the air filter and the fuel control unit was collapsed due to disbonding of the internal supporting wire. It could not be determined if this had occurred prior to the ditching and was the cause of the power loss, or had occurred due to the forces/pressure of the water in the engine bay during the ditching. No other anomalies were found that could have caused the power loss. The air duct hose was one that is commonly called a 'SCAT' hose and was made up of a single layer of neoprene impregnated fabric material supported internally by a spring steel helix wire bonded to the fabric. This SCAT hose is not appproved by the manufacturer for this installation. The correct hose carries the manufacturer's part number and is constructed of a 2 ply silicone resin impregnated with woven fibreglass which is bonded and cured along with an inner liner and tabbed ends to facilitate retention. It is also wire reinforced with galvanised hard temper spring steel. The manufacturer of the SCAT hose has recently changed the specification for these hoses to say that they are 'not recommended for negative pressure applications'. Many aircraft have SCAT or similar hoses fitted to negative pressure engine intake systems, as was the case with this aircraft.

Accident investigation:
cover
  
Investigating agency: BASI
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

https://www.atsb.gov.au/publications/investigation_reports/1997/aair/199700219/
https://www.atsb.gov.au/media/4930625/199700219.pdf

Revision history:

Date/timeContributorUpdates
01-May-2018 06:08 Pineapple Added

Corrections or additions? ... Edit this accident description

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