ASN Wikibase Occurrence # 210296
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Date: | Wednesday 30 August 2017 |
Time: | 18:08 |
Type: | Piper PA-31-350 Navajo Chieftain |
Owner/operator: | Star Marianas Air, Inc. |
Registration: | N4078J |
MSN: | 31-8152057 |
Year of manufacture: | 1980 |
Total airframe hrs: | 9341 hours |
Engine model: | Lycoming TIO-540-J2BD |
Fatalities: | Fatalities: 0 / Occupants: 7 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Saipan International Airport (SPN/PGSN) -
United States of America
|
Phase: | Take off |
Nature: | Unknown |
Departure airport: | Rota Airport (ROP/PGRO) |
Destination airport: | Saipan International Airport (SPN/PGSN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during the initial climb, about 150 ft above the ground, while the landing gear were being retracted, the airplane impacted a flock of medium-sized birds. He noted that the landing gear unlock indicator remained illuminated and that the landing gear handle would not return to the up neutral position. No degradation of performance was noted, so the pilot chose to continue to his destination.
About 20 miles from the airport, the pilot attempted to lower the landing gear but was unsuccessful. He contacted maintenance personnel on the ground and advised them of the landing gear issue. The ground maintenance personnel visually verified that the nose and right main landing gear (MLG) were down. The pilot performed the emergency gear extension checklist and noted little to no resistance on the hand pump. The pilot made multiple attempts to lower the landing gear without success. During the landing, the right MLG collapsed, and the left wing impacted the ground.
The airplane sustained substantial damage to the fuselage.
Postaccident examination revealed snarge on both horizonal stabilizers, the left wing, and the fuselage and that the right inboard MLG door actuator hose had failed.
Probable Cause: Impact with multiple birds while retracting the landing gear, which resulted in the subsequent failure of the right inboard main landing gear door actuator hose and prevented the pilot from being able to extend the landing gear.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA17CA570 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
01-May-2018 13:45 |
ASN Update Bot |
Added |
29-Oct-2019 17:11 |
Uli Elch |
Updated [Aircraft type, Narrative] |
22-Sep-2023 19:55 |
harro |
Updated [[Aircraft type, Narrative]] |
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