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ASN Wikibase Occurrence # 211470
Last updated: 19 July 2021
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Time:12:45 LT
Type:Silhouette image of generic ST75 model; specific model in this crash may look slightly different
Boeing E75 Stearman
Owner/operator:Vintage Aeroplane Collection #2 Inc
Registration: N43YP
MSN: 76-6018
Fatalities:Fatalities: 0 / Occupants: 1
Other fatalities:0
Aircraft damage: Substantial
Location:Turweston Aerodrome, Buckinghamshire -   United Kingdom
Phase: Take off
Departure airport:Turweston Aerodrome (EGBT)
Destination airport:
Investigating agency: AAIB
Substantially damaged 26/5/2018 at Turweston Aerodrome, Buckinghamshire: The aircraft appeared to lose power and attempted to return to the airport shortly after taking off. The runway in use at the time was 09 and the plane came to rest parallel to the 27 threshold facing south

The same aircraft had previously been damaged in a ground loop on landing at North Weald Airfield, Essex, on 13/4/2016.

UPDATE: The official AAIB report into the incident was published on 8 December 2018, and the following is an excerpt from it...

"Boeing Stearman, N43YP: Forced landing following power loss during initial climb, Turweston Aerodrome, Buckinghamshire, 26 May 2018.

The pilot reported that, prior to departure, he operated the engine at full throttle and achieved an engine speed of 1,900 rpm with almost imperceptible ‘mag-drop’. On applying full carburettor heat there was a 50 rpm engine speed reduction.

Shortly after takeoff, at approximately 100 ft, there was a sudden and complete loss of power. The pilot briefly considered landing ahead in a crop field but judged that this would almost certainly cause the aircraft to overturn. The position of the fuel tank within the centre section of the upper wing influenced his thinking. He therefore attempted to turn back and land in the downwind direction, albeit with limited confidence in a successful outcome. The aircraft struck the ground in a left wing-low attitude with a significant sink rate and was substantially damaged.

During a subsequent visit to the site, the pilot examined the crop field beyond the airfield boundary. He noted that it contained a tall bean crop and he felt that this confirmed his decision that a forced landing ahead would have been more hazardous."

Damage sustained to airframe: Per the above AAIB report, the aircraft sustained "extensive damage". However, the AAIB report goes on to state..."Although the aircraft was extensively damaged, a decision was made to repair it. The engine will be sent to an overhaul facility for strip examination, shock-load inspection and replacement of any damaged components. The fuel system will also be examined closely."


1. AAIB report:
2. FAA Registration:

Accident investigation:
Investigating agency: AAIB
Status: Investigation completed
Duration: 6 months
Download report: Final report


The aircraft being winched out of its resting position

Revision history:

26-May-2018 17:33 Aviatoruk Added
26-May-2018 20:09 Geno Updated [Cn, Operator, Location, Source]
26-May-2018 20:09 GAFlyer Updated [Total fatalities, Total occupants, Other fatalities, Phase, Nature, Departure airport, Source, Narrative]
26-May-2018 20:30 Dr. John Smith Updated [Time, Cn, Operator, Location, Departure airport, Source, Narrative]
27-May-2018 06:25 aviatoruk Updated [Source, Narrative, Photo, ]
27-May-2018 22:37 TB Updated [Operator, Source]
30-May-2018 09:47 aviatoruk Updated [Source]
06-Dec-2018 17:54 Dr.John Smith Updated [Time, Source, Narrative]
06-Dec-2018 17:59 Dr.John Smith Updated [Narrative]
06-Dec-2018 18:05 Dr.John Smith Updated [Narrative]
06-Dec-2018 19:31 harro Updated [Source, Accident report, ]

Corrections or additions? ... Edit this accident description