ASN Wikibase Occurrence # 211545
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Date: | Sunday 27 May 2018 |
Time: | 18:18 |
Type: | Piper PA-28-140 Cherokee |
Owner/operator: | Private |
Registration: | N95410 |
MSN: | 28-25930 |
Year of manufacture: | 1969 |
Total airframe hrs: | 3885 hours |
Engine model: | Lycoming O-320-E2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Pendleton County, NW of Falmouth, KY -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Kennett, MO (TKX) |
Destination airport: | Columbus, OH (TZR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while en route, the airplane’s engine began to run roughly and lose power. He immediately turned toward the nearest airport and slowed the airplane to 100 knots. He added that he pushed the mixture to full rich, which caused a short burst of power that lasted just a few seconds. He then pumped the throttle and applied carburetor heat but then realized he did not have enough altitude to make the airport and began to look for an alternate landing site.
The pilot further added that, after locating a ridgetop field, he slowed the airplane to 75 knots and pulled one notch of flaps and trimmed for landing. As he lined the airplane up with the field, he pulled full flaps about 300 ft above the ground. The touchdown was smooth, and the airplane continued the landing roll in 3-ft-tall wheat. Subsequently, the right wing struck an industrial irrigation nozzle, and the right wing separated from the fuselage.
The airplane sustained substantial damage to the right wing and stabilator.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
The pilot added that, during the engine failure, he did not attempt to change the fuel tank from the empty right wing fuel tank and recommended to make the fuel selector check the first part of the restart procedure.
The Federal Aviation Administration inspector reported that, while on scene, he was able to run the engine. He added that the left tank was about 1/2 full of fuel. He switched the fuel selector to the left tank and started the engine normally. The oil pressure was fine; the fuel pressure was normal on both the electric pump and engine-driven pump; and the magnetos checked fine.
Probable Cause: The pilot’s improper fuel management, which resulted in fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA18CA307 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=95410 Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
28-May-2018 04:57 |
Geno |
Added |
29-May-2018 17:56 |
harro |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
11-Nov-2018 08:31 |
ASN Update Bot |
Updated [Time, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
11-Nov-2018 08:49 |
harro |
Updated [Source, Narrative, Photo] |
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