Loss of control Accident Aero Commander 500S Shrike Commander N411JT,
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ASN Wikibase Occurrence # 21430
 
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Date:Tuesday 24 June 2008
Time:10:20
Type:Silhouette image of generic AC50 model; specific model in this crash may look slightly different    
Aero Commander 500S Shrike Commander
Owner/operator:Central Air Southwest
Registration: N411JT
MSN: 3097
Year of manufacture:1971
Total airframe hrs:12427 hours
Engine model:Lycoming IO-540-E1B5
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:S of Tonganoxie, Kansas -   United States of America
Phase: En route
Nature:Training
Departure airport:Kansas City, MO (MKC)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline's chief pilot was giving a newly-hired pilot a required competency/proficiency check. Memory data from the airplane's global positioning system showed the airplane made steep 360-degree turns to the left and right before continuing towards a practice area at gradually decreasing airspeed and altitude. A low cloud ceiling prevailed. Witnesses said they heard both engines "sputter, then quit," and saw the airplane clear a grove of trees, stall, and strike the ground. The landing gear was down and the flaps were in the approach setting. Both propellers were in the low pitch/high rpm setting, and bore little rotational signatures. Both engine fuel supply lines contained only residual fuel. Those familiar with the chief pilot's flying practices stated that he always followed a certain routine when giving a check ride. The routine consisted of the following: After performing steep 360-degree turns, he would ask the trainee to configure the airplane for landing and demonstrate minimum control maneuvers. Prior to executing steep turns, he would turn the boost pumps on. At the completion of the maneuver, the pumps would be turned off. The investigation revealed that there are unguarded fuel shutoff switches next to the boost pumps, and the circumstances of the accident are consistent with the these fuel shutoff switches being inadvertently placed in the off position, instead of the fuel boost pumps.
Probable Cause: The pilot-in-training inadvertently shutting off both engine fuel control valves causing a loss of power in both engines, and the pilot's failure to maintain control of the airplane resulting in a stall. Contributing to the accident was the chief pilot's inadequate supervision of the pilot-in-training.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN08FA114
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
24-Jun-2008 23:25 Fusko Added
25-Jun-2008 09:48 Dmitriy Updated
26-Jun-2008 05:27 JINX Updated
26-Jun-2008 10:18 Donaldopato Updated
12-Jul-2008 02:35 Fusko Updated
12-Jul-2008 12:41 Fusko Updated
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
03-Dec-2017 11:22 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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