Incident Boeing 717-200 N910ME,
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ASN Wikibase Occurrence # 217211
 
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Date:Thursday 12 May 2005
Time:23:16
Type:Silhouette image of generic B712 model; specific model in this crash may look slightly different    
Boeing 717-200
Owner/operator:Midwest Airlines
Registration: N910ME
MSN: 55174/5124
Total airframe hrs:4806 hours
Fatalities:Fatalities: 0 / Occupants: 80
Aircraft damage: None
Category:Incident
Location:Union Star, MO -   United States of America
Phase: En route
Nature:Passenger - Scheduled
Departure airport:Kansas City, MO (MCI)
Destination airport:Washington, DC (DCA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After departure, the incident airplane was climbing toward its cruising altitude in a stratified region of precipitation within a convective system, and in conditions which were favorable for the accumulation of structural icing. At some point, the pitot/static system began accumulating ice because the air data heat system had not been activated or was not functioning. The condition first manifested itself as a "RUDDER LIMIT FAULT" warning due to icing of the rudder limiting system pitot tube. The icing continued to accumulate on the other probes of the air data system, degrading its ability to reliably determine the airplane's airspeed. About 19,000 feet, the flight crew disengaged the autopilot and pushed the pitch control column forward, and the airplane entered a descent. The flight crew initially applied uncoordinated control inputs, in the process reaching nearly 100 pounds of differential force on the pitch control column, while attempting to recover the airplane. During this period, airplane's pitch continued to oscillate through 5 cycles, for duration of 8 minutes, reaching altitudes as low as 10,600 feet and as high as 23,300 feet. During the oscillations the airplane's indicated airspeed varied greatly, between 54 and 460 knots; however, the airplane systems tests and aircraft performance data show that the recorded, as well as the displayed, airspeed indications were adversely affected by the icing conditions. Once regaining control of the airplane, the crew diverted and made an uneventful landing. Post-incident testing of the airplane's mechanical and electronic systems revealed no abnormalities that would have accounted for the unreliable airspeed indications or the loss of control reported by the flight crew. Post-incident computer modeling also confirmed that the airplane performed in a manner consistent with all deviations from normal flight having been initiated or exacerbated by the control inputs of the flight crew. Review of flight data recorder, cockpit voice recorder, and flight crew interviews revealed that the flight crew's actions during the event were in part contradictory with operator's training and operational procedures. Specifically, the crew initially failed to properly identify and respond to the erroneous airspeed indications that were presented and failed to coordinate their recovery of the airplane to controlled flight.

Probable Cause: A loss of reliable airspeed indication due to an accumulation of ice on the air data/pitot sensors. Contributing to the incident was the flight crew's improper response to the erroneous airspeed indications, their lack of coordination during the initial recovery of the airplane to controlled flight, and icing conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050523X00653&key=1

Location

Revision history:

Date/timeContributorUpdates
03-Nov-2018 20:41 ASN Update Bot Added

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