ASN Wikibase Occurrence # 217291
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Date: | Sunday 4 November 2018 |
Time: | 09:33 |
Type: | Cessna 150E |
Owner/operator: | Private |
Registration: | N3515J |
MSN: | 15061215 |
Year of manufacture: | 1965 |
Total airframe hrs: | 2586 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Air Acres Airport (5GA4), Woodstock, GA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Woodstock, GA (5GA4) |
Destination airport: | Woodstock, GA (5GA4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot and student pilot passenger were departing on a local personal flight from a 2,000-ft-long turf runway. The passenger reported that the airplane seemed to "struggle to climb" after clearing trees near the end of the runway. He heard the stall warning horn activate, and the airplane descended into trees and impacted the ground. Witnesses reported that the airplane "wobbled" as it climbed and that the right wing dropped before the airplane crashed into the woods.
Although the airplane's most recent annual inspection was completed about 8 years before the accident, examination of the airframe and engine did not reveal any evidence of a preaccident malfunction or anomaly. A review of the pilot's logbook revealed no current flight review or recent flight experience, and the pilot did not hold a current medical certificate. Reported wind conditions at a nearby airport indicated that a quartering tailwind may have been present about the time of the accident, with gusts up to 20 knots. Based on the available information, it is likely that the pilot failed to maintain airspeed during the initial climb in gusting wind conditions, which resulted in an exceedance of the airplane's critical angle of attack, an aerodynamic stall, and loss of control.
Probable Cause: The pilot's failure to maintain airspeed during the initial climb in gusting wind conditions, which resulted in an aerodynamic stall and loss of control. Contributing to the accident was the pilot's lack of recent flight experience.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA19LA037 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=3515J%20 Location
Revision history:
Date/time | Contributor | Updates |
04-Nov-2018 21:08 |
Geno |
Added |
06-Nov-2018 03:42 |
Geno |
Updated [Registration, Cn, Operator, Source] |
07-Nov-2018 06:41 |
Anon. |
Updated [Aircraft type] |
22-Apr-2020 17:01 |
ASN Update Bot |
Updated [Time, Operator, Total fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
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