Accident Grumman G-164A Ag-Cat N7395,
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ASN Wikibase Occurrence # 21737
 
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Date:Saturday 12 July 2008
Time:09:59
Type:Silhouette image of generic G164 model; specific model in this crash may look slightly different    
Grumman G-164A Ag-Cat
Owner/operator:Flynts Crop Dusting
Registration: N7395
MSN: 942
Year of manufacture:1972
Total airframe hrs:4557 hours
Engine model:Pratt & Whitney R1340
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:near Highway 93, Mitchell County, GA -   United States of America
Phase: En route
Nature:Agricultural
Departure airport:Pelham, GA
Destination airport:Pelham, GA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Approximately 2 weeks before the accident, significant unplanned maintenance was performed on the radial engine of the aerial application airplane. The activity included the removal of seven of the nine cylinders to remove fragments of piston rings, a piston skirt, and a broken governor drive gear from the engine case. Six of the removed cylinders were re-installed, and one cylinder was replaced with an overhauled cylinder and a new piston. The airplane was test flown, returned to service, and utilized for several days. On the day of the accident, one witness said that the engine was making "popping" noises before it crashed. The airplane touched down in a small clearing, but nosed over and collided with shrubs and trees. The accident site was located between the field being sprayed and the owner's airstrip. The pilot was fatally injured. Post-mortem toxicology revealed evidence of recent use of several over-the-counter, and one prescription, medications, but these medications are not typically associated with impairment. An autopsy revealed the presence of severe coronary artery disease and heart enlargement. The pilot’s physique and heart enlargement also strongly suggested that he may have suffered from obstructive sleep apnea, a condition associated with increased accident risk, but the circumstances of the accident were not consistent with impairment or incapacitation. Post accident examination of the engine revealed internal damage consistent with the engine being operated with one or more loose metallic items inside the engine case, but the damage could not be directly associated with the engine power loss. Several piston ring fragments were recovered from the engine case, but it could not be determined whether they were vestiges of previous problems, or were portions of the rings recently installed. No specific engine failure cause or mode was identified during the investigation.
Probable Cause: A partial loss of engine power for undetermined reasons which led to a forced landing in unsuitable terrain.

Accident investigation:
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Investigating agency: NTSB
Report number: NYC08LA245
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
14-Jul-2008 23:18 Fusko Added
03-Dec-2017 13:00 ASN Update Bot Updated [Time, Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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