Accident Beechcraft A36 Bonanza N2021T,
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ASN Wikibase Occurrence # 220903
 
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Date:Thursday 17 January 2019
Time:17:50 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Big Fuga LLC
Registration: N2021T
MSN: E-1325
Year of manufacture:1978
Total airframe hrs:3940 hours
Engine model:Lycoming TSIO-540
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:near Gillespie County Airport (T82), Fredericksburg, TX -   United States of America
Phase: En route
Nature:Private
Departure airport:San Antonio, TX (1T8)
Destination airport:San Antonio, TX (1T8)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The accident pilot was in cruise flight in a single-engine airplane when he declared "mayday" on the radio, stating the airplane's engine was on fire. The accident airplane impacted a field, crossed a road, and came to rest upright. A postcrash fire consumed the majority of the airframe.

The airplane was equipped with a turbo-charged reciprocating engine and propeller that had been converted under a Supplemental Type Certificate (STC). The engine had accumulated 412.2 hours between the last overhaul and the last annual inspection. The last inspection was about three months before the accident.

An examination of the engine revealed fire damage and limited rotation. Disassembly of the engine revealed a broken camshaft and crankshaft. Metallurgical examination of the crankshaft revealed crack arrest marks in the crankshaft, consistent with fatigue, which initiated in the fillet radius at the forward end of the number 6 connecting rod journal. Multiple crack origins and prominent crack arrest lines were consistent with a relatively high stress associated with crack initiation. However, a reason for the high stress or fatigue initiation could not be determined based on the limited airplane records and the damage to the airplane.

Probable Cause: The loss of engine power due to fatigue failure of the crankshaft.

Accident investigation:
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Investigating agency: NTSB
Report number: CEN19LA055
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB CEN19LA055

Location

Images:


Photo: NTSB

Media:

Revision history:

Date/timeContributorUpdates
18-Jan-2019 05:43 Geno Added
18-Jan-2019 07:25 Iceman 29 Updated [Embed code]
18-Jan-2019 07:29 Iceman 29 Updated [Embed code]
18-Jan-2019 07:30 Iceman 29 Updated [Aircraft type, Source]
18-Jan-2019 20:57 SeanWagnerCFI Updated [Time]
01-May-2019 20:28 Captain Adam Updated [Aircraft type, Registration, Cn, Operator, Nature, Departure airport, Source, Narrative]
08-Sep-2020 12:43 ASN Update Bot Updated [Departure airport, Destination airport, Source, Embed code, Narrative]
31-Mar-2021 13:54 ASN Update Bot Updated [Time, Other fatalities, Source, Embed code, Narrative, Category, Accident report]
31-Mar-2021 14:08 harro Updated [Phase, Source, Embed code, Narrative, Photo]

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