ASN Wikibase Occurrence # 224440
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Date: | Saturday 27 April 2019 |
Time: | 15:00 LT |
Type: | Zenith CH 601 HDS Zodiac |
Owner/operator: | Private |
Registration: | N61PG |
MSN: | 63888 |
Year of manufacture: | 1999 |
Total airframe hrs: | 723 hours |
Engine model: | Rotax 912 ULS |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fuquay-Varina, Harnett County, NC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Carthage, NC (BQ1) |
Destination airport: | Fuquay/Angier, NC (NC78) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:About 10 nautical miles from the destination during a cross-country flight, the airplane's engine began to run rough, cut in and out, and surge. The pilot checked the header fuel tank level and noted that it was nearly full, and he activated the electrically driven fuel pump, but the engine issues continued. The airplane continued to lose altitude and the engine continued to run rough; about 1,000 ft above the ground and about two nautical miles from the destination airport, the pilot decided to reduce engine power to idle and complete a precautionary landing in a field. During the landing roll, the airplane impacted a dirt pile and nosed over, resulting in substantial damage to the fuselage, empennage, and wings.
Fuel was found in the bowls of both carburetors and in both wing tanks and the header tank. Examination of the engine found no preimpact mechanical malfunctions or failures that would have precluded normal operation, and when the engine was test run from an external fuel source using the engine-driven fuel pump, it started and produced power at multiple power settings.
Given the presence of fuel and the lack of anomalies found during the postaccident engine test run, it is possible that the fuel supply to the engine was partially interrupted, which resulted in the engine continuing to run rough to the extent that maintaining altitude was not possible; however, the reason for the interruption of the fuel supply could not be determined.
Probable Cause: A partial loss of engine power due to partial interruption of the fuel supply for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA19LA159 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=61PG NTSB ERA19LA159
Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
28-Apr-2019 01:17 |
Geno |
Added |
28-Apr-2019 05:17 |
RobertMB |
Updated [Aircraft type, Source] |
28-Apr-2019 05:30 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source, Narrative] |
28-Apr-2019 09:49 |
RobertMB |
Updated [Aircraft type, Location, Nature, Narrative] |
28-Mar-2021 14:06 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
28-Mar-2021 14:22 |
harro |
Updated [Source, Narrative, Photo] |
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