Fuel exhaustion Accident Cessna 172F Skyhawk N8559U, Saturday 27 January 2018
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Date:Saturday 27 January 2018
Time:01:20
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172F Skyhawk
Owner/operator:Private
Registration: N8559U
MSN: 17252459
Year of manufacture:1965
Total airframe hrs:4792 hours
Engine model:Continental O-300-C
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Aircraft damage: Destroyed
Category:Accident
Location:near Williamsport, IN -   United States of America
Phase: En route
Nature:Ferry/positioning
Departure airport:Columbus-Rickenbacker International Airport, OH (LCK/KLCK)
Destination airport:Danville-Vermilion County Airport, IL (DNV/KDNV)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On January 27, 2018, about 0121 eastern standard time, a Cessna 172F, N8559U, collided with trees and impacted terrain near Williamsport, Indiana. The commercial pilot was fatally injured. The airplane was registered to and operated by Kilo Aviation, LLC, Lacon, Illinois, under the provisions of Title 14 Code of Federal Regulations Part 91 as a ferry flight. Night visual meteorological conditions prevailed, and no flight plan had been filed. The flight originated from Rickenbacker International Airport (LCK), Columbus, Ohio, at 2130, and was destined for Vermilion Regional Airport (DNV), Danville, Illinois.

The commercial pilot was ferrying the newly-purchased airplane cross-country for the new owner. The first leg of the trip was completed without incident. After refueling the airplane, the pilot departed and proceeded toward the destination in night visual meteorological conditions. After about 3 hours, 51 minutes of flight, the airplane descended and impacted trees and terrain about 9 miles short of the destination. Examination of the wreckage revealed evidence of fuel exhaustion; both main fuel tanks were intact, no fuel was observed inside the tanks, and no fuel smell was noticed at the site. The lack of damage to the propeller blades was consistent with the engine not developing power at impact. According to the manufacturer's performance chart, with full main tanks, the airplane had an endurance of about 3.7 hours. Therefore, it is likely that the engine lost power as a result of fuel exhaustion.

Although toxicology testing was positive for opioids, the relative amounts of these opioids detected in urine suggest that the source may have been the ingestion of poppy seeds rather than pharmaceuticals.

Probable Cause: The pilot's mismanagement of fuel, which resulted in fuel exhaustion and descent and collision with trees.

Accident investigation:
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Investigating agency: NTSB
Report number: CEN18FA088
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB
https://data.ntsb.gov/Docket?ProjectID=96680

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
01-Jun-2019 07:29 ASN Update Bot Added
12-Mar-2025 15:33 Captain Adam Updated [Aircraft type, Location, Phase, Source, Narrative, Photo, ]

Corrections or additions? ... Edit this accident description

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