Accident Cessna T337G Pressurized Skymaster N1ZR,
ASN logo
ASN Wikibase Occurrence # 226202
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Thursday 8 November 2018
Time:c. 10:00
Type:Silhouette image of generic P337 model; specific model in this crash may look slightly different    
Cessna T337G Pressurized Skymaster
Owner/operator:Private
Registration: N1ZR
MSN: P337-0275
Year of manufacture:1977
Total airframe hrs:1879 hours
Engine model:Continental TSIO-520-NB16
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Homosassa, FL -   United States of America
Phase: Landing
Nature:Private
Departure airport:Memphis International Airport, TN (MEM/KMEM)
Destination airport:Brooksville-Hernando County Airport, FL (KBKV)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, 2 days before the accident flight, the Cessna T337G Pressurized Skymaster's fuel tanks were filled (150 gallons). During the taxi to the runway, the right main tire blew. During recovery, the right side of the airplane was placed on a dolly to support the gear so that the airplane could be towed. The pilot reported that, due to the airplane’s fuel system design, when one side of the airplane was raised, all the fuel could be transferred to the opposite tank, which then forced the fuel to be released out of the air vent line.
On the day of the accident, the pilot completed his preflight inspection and visually confirmed the fuel quantity by checking both fuel gauges, which were "green"; however, he did not verify the fuel onboard by checking the tanks. About 3 hours into the flight, the rear engine lost power. Before the pilot attempted to restart the rear engine and after he verified the correct engine to feather, the front engine also lost power. When the pilot realized the airplane would be unable to reach the nearest airport, he landed it in a grass marsh with the landing gear retracted. During the landing, the airplane’s wing hit grass and then veered right about 90°, which caused the left wing to dip and impact terrain.
The airplane sustained substantial damage to the left aileron and empennage.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
During his preflight inspection, the pilot should have verified the fuel quantity in the fuel tanks to ensure there was sufficient fuel onboard for the flight, and his failure to do so led to fuel exhaustion and the subsequent total loss of power in both engines.

Probable Cause: The pilot's inadequate preflight inspection, which resulted in fuel exhaustion and the subsequent total loss of power in both engines.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: GAA19CA070
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
15-Jun-2019 16:19 ASN Update Bot Added
15-Jun-2019 17:01 harro Updated [Aircraft type, Phase, Departure airport, Destination airport, Narrative]
15-Jul-2022 02:49 RobertMB Updated [Time, Aircraft type, Cn, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org