Accident Bell UH-1H ZS-HLJ,
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ASN Wikibase Occurrence # 227531
 
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Date:Tuesday 23 July 2019
Time:13:06
Type:Silhouette image of generic UH1 model; specific model in this crash may look slightly different    
Bell UH-1H
Owner/operator:Kishugu Aviation
Registration: ZS-HLJ
MSN: 8800
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Waterval Base, near Tzaneen, Limpopo -   South Africa
Phase: Initial climb
Nature:Fire fighting
Departure airport:Letaba Air Base
Destination airport:Letaba Air Base
Investigating agency: CAA S.A.
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On Tuesday 23 July 2019, two Bell UH-1H helicopters with registration marks ZS-HLJ and ZU-LCY, as well as a Spotter aircraft, a Cessna 182, were dispatched to a fire-fighting mission at Woodbush Forest Reserve near Tzaneen. Each aircraft dispatched with a pilot on-board. The ZS-HLJ pilot reported that after turning on course for Woodbush Forest Reserve at approximately 200 feet, he noticed a lack of engine power as the helicopter was struggling to climb. Thereafter, the pilot heard a loud bang coming from the engine compartment. Upon checking the instrument panel, he noted that both the rotor and engine revolutions per minute (rpm) were decreasing and that the master warning light had illuminated. The pilot broadcasted a Mayday call on frequency 123.55 megahertz (MHz) before partially lowering the collective; he further noted that the rotor rpm kept decreasing. The pilot then scanned the area for a possible landing site and identified an open area (to his right). He then fully lowered the collective and continued to descend to undertake a forced landing. The pilot attempted to flare the helicopter to cushion the landing, however, the aircraft landed hard and broke both skids; the main rotor blades severed the upper section of the tail boom. The helicopter sustained substantial damages and the pilot was not injured during the accident sequence.

Probable cause/s
Although the manufacturer’s technical report could not determine the cause of the engine failure, it is probable that the engine was periodically started at high temperature, and as a result of not being monitored during engine start, led to the development of fatigue cracks and the subsequent internal failures.

Accident investigation:
cover
  
Investigating agency: CAA S.A.
Report number: 
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

https://www.facebook.com/374787335874973/posts/2445824118771274/
ex.N205UE, EC-GDO, CC-CME.

https://www.airliners.net/photo/Working-On-Fire/Bell-UH-1H-Iroquois/5001671 (photo)

Media:

Revision history:

Date/timeContributorUpdates
24-Jul-2019 15:45 Anon. Added
24-Jul-2019 15:46 harro Updated [Operator, Nature, Embed code, Narrative]
24-Jul-2019 16:08 Geno Updated [Source]
24-Jul-2019 20:28 RobertMB Updated [Cn, Location, Source, Narrative]
25-Jul-2019 07:40 A.J.Scholten Updated [Source]
29-Jul-2019 11:37 Aerossurance Updated [Location, Phase, Narrative]
22-Sep-2020 10:32 Aerossurance Updated [Location]

Corrections or additions? ... Edit this accident description

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