ASN Wikibase Occurrence # 22790
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Date: | Tuesday 9 September 2008 |
Time: | 10:30 |
Type: | Mooney M20C |
Owner/operator: | Conley Raymond G |
Registration: | N21MY |
MSN: | 2522 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3921 hours |
Engine model: | Lycoming O&VO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near the Wallace Airport, Pender County, NC -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Wallace, NC (ACZ) |
Destination airport: | Norfolk, VA (ORF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reportedly performed a preflight inspection of the airplane using the airplane's checklist, and also performed an engine run-up before takeoff; no discrepancies were noted. The pilot applied power to take off and no discrepancies were noted. A witness reported hearing the engine running smooth but perceived it to be operating at a reduced power setting (estimated 60 percent power) during the takeoff roll. He advised the pilot on the common traffic advisory frequency to apply full power but he didn't respond. The witness saw the airplane become airborne just short of midfield, but noted that it was slow leaving the runway. Additionally, the airplane remained in ground effect for most of the remaining runway and climbed no higher than 100 feet above ground level. The pilot stated that when the flight was at that altitude, he experienced a sudden loss of engine power. He continued straight ahead past the departure end of the runway and executed a forced landing into the tops of trees. During recovery of the airplane, green colored foam and red colored lanyard material was found wedged against the engine baffling behind the propeller spinner bulkhead. No blockage of the air induction filter was noted. Following recovery of the airplane, a replacement propeller was installed and the engine was started and operated to full power as indicated by the tachometer with no discrepancies noted. Following the engine run, red colored lanyard consistent with that used as a streamer for the engine cowling ram air inlet plugs was found on top of the engine cylinders.
Probable Cause: The pilot's failure to abort the takeoff when the engine failed to develop full power. Contributing to the accident was the pilot's failure to remove the intake plugs prior to takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA08LA188 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
11-Sep-2008 10:54 |
jorgetadeu7 |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 12:07 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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