ASN Wikibase Occurrence # 228428
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Date: | Thursday 22 August 2019 |
Time: | 19:39 |
Type: | Cessna A185F Skywagon |
Owner/operator: | Acadian Seaplanes, LLC |
Registration: | N1920Q |
MSN: | 18503502 |
Year of manufacture: | 1977 |
Total airframe hrs: | 2582 hours |
Engine model: | Continental IO–520–D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rangeley Lake Seaplane Base, Franklin County, ME -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Rangeley, ME (M57) |
Destination airport: | Bangor International Airport, ME (BGR/KBGR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while departing from a lake, the float-equipped airplane was not "gaining airspeed as usual" and that the takeoff run was taking "longer." Before attempting to abort the takeoff, the left float lifted off the water, followed by the right float. While in ground effect, the floatplane started to roll right. The pilot corrected with full left aileron, but the floatplane continued to roll right. He then reduced power and applied 40º of flaps, but the floatplane continued to roll right, so he increased the throttle to full, and the right wing impacted the water. The airplane sustained substantial damage to the right wing. The pilot reported that the floatplane impacted rocks while he was back taxiing to the dock after a previous flight but that he did not realize the floats had been damaged. Before the accident flight, he conducted a preflight inspection and did not find any residual water in the floats, but he did not examine the bottom of the floats because they were submerged in water. Photographs showed that the right float’s keel was damaged.
Probable Cause: The pilot's inadequate preflight inspection of the floats, which led to his subsequent attempt to depart from a lake with damaged floats and led to a loss of roll control and the right wing impacting the water.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA19CA513 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=1920Q
History of this aircraft
Other occurrences involving this aircraft Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
22-Aug-2019 22:13 |
Captain Adam |
Added |
22-Aug-2019 22:24 |
Geno |
Updated [Location, Departure airport] |
22-Aug-2019 23:37 |
RobertMB |
Updated [Time, Aircraft type, Registration, Cn, Operator, Destination airport, Source, Narrative] |
23-Aug-2019 16:10 |
RobertMB |
Updated [Registration, Source, Narrative] |
23-Aug-2019 16:11 |
RobertMB |
Updated [Time] |
23-Mar-2020 18:42 |
ASN Update Bot |
Updated [Time, Cn, Operator, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
23-Mar-2020 18:51 |
harro |
Updated [Destination airport, Source, Narrative, Photo, Accident report, ] |
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