ASN Wikibase Occurrence # 228583
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Date: | Wednesday 28 August 2019 |
Time: | 19:10 LT |
Type: | Cessna 172P Skyhawk II |
Owner/operator: | Rocky Mountain Flight School |
Registration: | N53432 |
MSN: | 17274748 |
Year of manufacture: | 1981 |
Engine model: | Lycoming O-320 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rocky Mountain Metropolitan Airport (BJC/KBJC), Broomfield, CO -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Colorado Springs Municipal Airport, CO (COS/KCOS) |
Destination airport: | Denver, CO |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot was completing a solo cross-country flight when he noticed the low voltage warning light illuminate; however, since the voltmeter continued to indicate about 28 volts (v), he continued the flight to the destination airport and completed a touch-and-go landing before proceeding back to the departure airport. The pilot later stated that he was 'not confident that he completely understood how an electrical system failure may affect the aircraft.' As the pilot attempted to lower the flaps before landing, the airplane experienced a complete loss of electrical power, and the flaps did not extend.
The student pilot conducted a no-flap landing to the 3,600-ft-long runway, during which the airplane bounced multiple times and continued off the end of the runway and over a retaining wall, resulting in substantial damage. The pilot reported that he had not received training in no-flap landings.
Examination of the alternator revealed no anomalies that would have precluded normal operation. Some wiring associated with the alternator displayed areas of broken insulation and exposed wire; however, it could not be determined if this was due to preaccident chafing or the result of impact damage. Based on the available information, the reason for the loss of electrical power could not be determined.
Probable Cause: A total loss of electrical power for reasons that could not be determined, and the student pilot's subsequent runway overrun during a no-flap landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA292 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA292
https://flightaware.com/live/flight/N53432/history/20190829/0032Z/KBJC/KBJC
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
29-Aug-2019 03:28 |
Geno |
Added |
29-Aug-2019 03:30 |
Geno |
Updated [Aircraft type, Operator, Source] |
29-Aug-2019 05:39 |
RobertMB |
Updated [Registration, Narrative] |
29-Aug-2019 10:42 |
RobertMB |
Updated [Location, Source, Narrative] |
29-Aug-2019 11:45 |
RobertMB |
Updated [Operator] |
07-Sep-2019 14:48 |
Geno |
Updated [Phase, Nature, Departure airport, Destination airport, Narrative] |
01-Jul-2022 18:44 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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