Accident Diamond DA40NG Diamond Star N292RA,
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ASN Wikibase Occurrence # 229068
 
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Date:Sunday 15 September 2019
Time:16:50 LT
Type:Silhouette image of generic DA40 model; specific model in this crash may look slightly different    
Diamond DA40NG Diamond Star
Owner/operator:Private
Registration: N292RA
MSN: 40.NC033
Year of manufacture:2018
Total airframe hrs:123 hours
Engine model:Austro Engines E4-A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:NW of Chesapeake Regional Airport (KCPK), Norfolk, VA -   United States of America
Phase: Landing
Nature:Private
Departure airport:Norfolk-Chesapeake Regional Airport, VA (KCPK)
Destination airport:Norfolk-Chesapeake Regional Airport, VA (KCPK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that, shortly after takeoff, he heard a noise from under the engine cowling followed by a partial loss of engine power. The pilot was unable to maintain altitude and made a forced landing to a field, which resulted in substantial damage to the fuselage.
Data downloaded from the airplane's electronic engine control unit was consistent with an uncommanded decrease in induction air boost pressure on takeoff. Postaccident examination of the engine revealed that the flexible induction coupling between the intercooler and the engine induction inlet had backed off. The two clamps that secured the flexible coupling to the induction inlet were intact and safety wired. However, the two clamps were loose, and the induction tube could be inserted into the coupling without loosening the clamps. A review of maintenance records revealed that the flexible induction coupling and clamps had been removed and replaced at the last 100-hour inspection about 15 flight hours before the accident. Because the two clamps that secured the coupling from the intercooler to the induction inlet were recently replaced, it is likely that the mechanic who installed the clamps did not properly tighten them, and they loosened in flight, leading to the induction inlet backing off and resulting in a loss of engine power.


Probable Cause: A partial loss of engine power due to the mechanic's failure to properly tighten the two clamps securing the flexible coupling from the intercooler to the induction inlet.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA19LA272
Status: Investigation completed
Duration:
Download report: Final report

Sources:

FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=292RA

NTSB ERA19LA272

Location

Revision history:

Date/timeContributorUpdates
15-Sep-2019 22:39 Geno Added
15-Sep-2019 23:47 RobertMB Updated [Aircraft type, Nature, Source]
16-Sep-2019 14:26 RobertMB Updated [Registration, Cn, Operator, Source, Damage, Narrative]
27-Mar-2021 06:58 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]
27-Mar-2021 07:29 harro Updated [Departure airport, Destination airport, Source, Narrative]

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