ASN Wikibase Occurrence # 234395
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Date: | Wednesday 25 March 2020 |
Time: | 18:30 LT |
Type: | Cessna 150E |
Owner/operator: | HAL Logistics LLC |
Registration: | N4729U |
MSN: | 15061177 |
Year of manufacture: | 1965 |
Total airframe hrs: | 3832 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Aero Country Airport (T31), McKinney, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | McKinney, TX (T31) |
Destination airport: | McKinney, TX (T31) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot conducted a preflight inspection of the airplane and estimated that he had about 14 gallons of fuel on board before departure based on measuring the fuel in the tanks with a dipstick. He then completed a 1-hour, round-trip flight during which he conducted three touch-and-go landings at the first destination, then returned to the departure airport and completed three more touch-and-go landings. During climbout after the third landing, the engine experienced a total loss of power. The pilot was unable to restart the engine and made a forced landing to a golf course; the airplane collided with a tee box and nosed over, resulting in substantial damage to the airplane's wings, forward fuselage, vertical stabilizer, and rudder.
While the airplane was inverted, fuel was leaking from the fuel tank caps, but the fuel caps remained intact and secured. After the airplane was flipped upright, 2 to 3 gallons of fuel were drained from the tanks. The airplane's unusable fuel is 3.5 gallons.
Postaccident examination of the airplane revealed no evidence of fuel in the rest of the fuel system and no other pre-accident anomalies that would have precluded normal operation. Based on that lack of usable fuel in the fuel system, it is likely that the pilot's inadequate preflight planning and inflight fuel management resulted in a total loss of engine power due to fuel exhaustion.
Probable Cause: The pilot's inadequate preflight fuel planning and inflight fuel management, which resulted in fuel exhaustion and a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20LA133 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB CEN20LA133
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N4729U Location
Revision history:
Date/time | Contributor | Updates |
26-Mar-2020 02:30 |
Captain Adam |
Added |
26-Mar-2020 15:24 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
20-Jun-2021 17:08 |
aaronwk |
Updated [Time, Nature, Destination airport, Source, Narrative] |
08-Jul-2022 09:27 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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