ASN Wikibase Occurrence # 235298
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Date: | Saturday 2 July 2016 |
Time: | 02:30 |
Type: | Bell OH-58A Kiowa |
Owner/operator: | Farm Aviation Inc |
Registration: | N6251G |
MSN: | 40995 |
Year of manufacture: | 1970 |
Total airframe hrs: | 13688 hours |
Engine model: | AMA/EXPR UNKNOWN ENG |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Brawley, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Brawley, CA |
Destination airport: | Brawley, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot reported that, after departing for the agricultural flight, he maneuvered the helicopter to line up with the field to be sprayed. Shortly after lining up with the field, the engine started to surge, and he saw the torque meter needle "bouncing rapidly." The pilot initiated a precautionary landing to an open field. The helicopter landed hard, which resulted in substantial damage to the tailboom and tail rotor drive shaft.
A test run of the engine revealed that the bleed valve did not close at any speed and that the engine produced less than 250 horsepower (hp). The bleed valve was disassembled, and the diaphragm was found to have several holes and cracks, and the poppet valve located in the bleed valve assembly had radial play, consistent with worn bushings. The damaged bleed valve was replaced with an overhauled bleed valve, and during a subsequent test run, the engine produced about 380 hp, which is about 7% below minimum allowable power for a serviceable engine. Given these results, the excessive wear of the bleed valve likely prevented it from closing during the accident flight, which resulted in the engine's degraded performance.
According to the operator, the compressor, turbine, and bleed valve assemblies were overhauled about 2 years before the accident and then reassembled on the engine. The engine had operated about 766 hours since overhaul at the time of the accident. The engine manufacturer reported that the bleed valve assembly should be overhauled every 1,500 hours. No component log cards or historical information for the bleed valve was located during the investigation.
According to the engine manufacturer, the bleed valve exhibited wear that was not consistent with a bleed valve with comparable service time. Therefore, it is likely that the bleed valve was likely not overhauled 2 years before the accident as reported by the operator and that it was beyond the overhaul period of 1,500 hours, which resulted in the observed wear that ultimately prevented the engine from producing sufficient power during takeoff.
Probable Cause: The engine's degraded performance due to excessive wear of the engine bleed valve, which prevented it from closing during the accident flight. Contributing to the accident was the operator's failure to overhaul the bleed valve within the manufacturer-recommended interval.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR16LA134 |
Status: | Investigation completed |
Duration: | 3 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
20-Apr-2020 07:37 |
ASN Update Bot |
Added |
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