ASN Wikibase Occurrence # 237716
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Date: | Sunday 5 July 2020 |
Time: | 11:24 LT |
Type: | Boeing B75 |
Owner/operator: | Air Museum |
Registration: | N61445 |
MSN: | 75-1335 |
Year of manufacture: | 1941 |
Total airframe hrs: | 7840 hours |
Engine model: | Pratt & Whitney R-985 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chino Airport (CNO/KCNO), CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Chino Airport, CA (CNO/KCNO) |
Destination airport: | Chino, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the tailwheel equipped biplane reported that, during a landing roll on runway 26R, the left wing 'dipped' and that he applied right aileron to counteract. The pilot stated that the airplane began to turn to the right and that, despite the application of full left rudder, left brake, and a brief application of power, he was unable to correct the movement. The lower left wing subsequently struck the ground. The airplane then veered sharply to the right, exited the runway, and the left main landing gear collapsed as the airplane came to rest upright.
Postaccident examination of the airplane revealed that the fuselage was structurally damaged. The left rudder/tailwheel cable idler arm was found fractured. Examination of the two pieces of fractured left rudder/tailwheel cable idler arm revealed that the fracture progressed though the section due to a monotonic bending load. It's likely that the fracture occurred during the pilot's attempt to counteract the airplane's movement to the right when directional control was lost.
The airport's automated weather observation station reported that, about 4 minutes after the accident, the wind was calm. However, the pilot reported that while on short final to the runway, the air traffic control tower controller reported wind was from 270° at 4 knots.
Probable Cause: The pilot's failure to maintain directional control during the landing roll.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR20LA226 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB WPR20LA226
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N61445
History of this aircraft
Other occurrences involving this aircraft
20 May 2016 |
N61445 |
(Planes of Fame) Air Museum |
0 |
Gillespie Field Airport (KSEE), San Diego/El Cajon, CA |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
07-Jul-2020 16:18 |
Captain Adam |
Added |
15-Jul-2022 11:03 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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