Accident Stoddard Hamilton Glasair III N713MJ, Tuesday 20 October 2020
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Date:Tuesday 20 October 2020
Time:17:10
Type:Silhouette image of generic GLAS model; specific model in this crash may look slightly different    
Stoddard Hamilton Glasair III
Owner/operator:Private
Registration: N713MJ
MSN: 3285
Engine model:Lycoming IO-540
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Aircraft damage: Substantial
Category:Accident
Location:Ford Heights, IL -   United States of America
Phase: En route
Nature:Private
Departure airport:Chicago-Lansing Municipal Airport, IL (KIGQ)
Destination airport:Chicago-Lansing Municipal Airport, IL (KIGQ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was on a local flight and his flight track indicated he was returning to his departure airport when the accident occurred. A witness reported seeing the airplane at a low altitude 'dragging' a light pole across the highway. The airplane then impacted the highway and came to rest in a wooded area alongside the road. Another witness reported that it sounded like the engine lost power and momentarily regained power before losing it again.

The wing fuel tanks were breached in the accident, and the amount of fuel on board could not be determined.

The two-bladed, constant speed propeller remained attached to the engine. One blade had minimal damage, the second blade's tip was bent back, starting about mid-span, and the leading edge was rough; this damage was consistent with the propeller not rotating at the time of impact. The engine was equipped with an electric ignition system and was unable to be field tested. The engine examination did not identify any preimpact anomalies that would affect engine operation.
 
The witness statement and signatures on the propeller are consistent with a loss of engine power; however, a reason for the loss of engine power could not be determined based on the available evidence.

Reviewed records show that ketamine was administered to the pilot after the crash. Thus, the postmortem toxicology results provide no evidence of any pre-crash use of potentially impairing substances by the pilot.

Probable Cause: The loss of engine power for reasons that could not be determined based on the available evidence.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN21FA024
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB CEN21FA024

https://data.ntsb.gov/Docket?ProjectID=102171
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult
https://flightaware.com/live/flight/N713MJ

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
21-Oct-2020 05:43 Geno Added
21-Oct-2020 06:01 Geno Updated [Location, Source, ]
21-Oct-2020 07:08 harro Updated [Registration, ]
21-Oct-2020 13:23 gerard57 Updated [Total fatalities, Source, Narrative, ]
10-Jul-2021 09:41 aaronwk Updated [Time, Phase, Departure airport, Destination airport, Source, Narrative, Category, ]
07-Jul-2022 19:09 ASN Update Bot Updated [Time, Other fatalities, Nature, Source, Narrative, Accident report, ]
08-Jul-2022 18:43 Captain Adam Updated [Time, Other fatalities, Phase, Source, Narrative, Photo, ]
23-Dec-2024 21:54 Captain Adam Updated [Location, Source, ]

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