Accident Lake LA-4-200 Buccaneer N2989P,
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ASN Wikibase Occurrence # 253866
 
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Date:Wednesday 21 April 2021
Time:13:10 LT
Type:Silhouette image of generic LA4 model; specific model in this crash may look slightly different    
Lake LA-4-200 Buccaneer
Owner/operator:EJH Teton Properties LLC
Registration: N2989P
MSN: 954
Year of manufacture:1979
Total airframe hrs:1737 hours
Engine model:Lycoming IO-360-A1B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:near Twentynine Palms Airport (TNP/KTNP), CA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Twentynine Palms, CA
Destination airport:Glendale Municipal Airport, AZ (KGEU)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had recently purchased the airplane and was transporting it to his home airport. During the cross-country flight, the pilot stopped to refuel the airplane. During departure, the airplane climbed to an altitude of about 200 ft above ground level, at which point the engine lost partial power and was unable to maintain altitude. The pilot elected to perform an emergency off-airport landing, and the airplane touched down on desert terrain. During the landing, the airplane collided with a sign and nosed over, coming to rest inverted.

The airplane had undergone a pre-buy and an annual inspection about 10 flight hours before the accident. The pilot stated that, on the day before the accident, he flight tested the airplane, during which time the manual turbocharger went into overboost for “a second' before he pulled the power back.

A postaccident examination revealed that several ceramic cores of the spark plugs were cracked. The combustion chambers were free from deposits, consistent with a preignition or detonation event. It is unknown if the overboost event that the pilot described resulted in this damage.

The magnetos, while still installed on the engine, did not produce a consistent spark, and their timing could not be determined. The magnetos were then removed from the engine. The right magneto was functionally tested and operated normally. The left magneto capacitor lead insulation had previously been cut, exposing the center conductor wire, consistent with improper assembly. The contact point tungsten faces were both corroded and exhibited an oxide crust on the external surfaces of the tungsten. A functional test, revealed the left magneto would not produce spark at different rpms. The left magneto was likely not operating during the accident takeoff, which, along with the cracked spark plugs, would have resulted in a partial loss of engine power.

Probable Cause: A partial loss of engine power due to inadequate ignition from cracked spark plugs and a failed magneto.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR21LA171
Status: Investigation completed
Duration: 2 years 1 month
Download report: Final report

Sources:

NTSB WPR21LA171
https://flightaware.com/live/flight/N2989P

Location

Revision history:

Date/timeContributorUpdates
24-Apr-2021 17:07 Captain Adam Added
24-Apr-2021 17:29 RobertMB Updated [Source]
11-Jun-2023 08:17 ASN Update Bot Updated [[Source]]

Corrections or additions? ... Edit this accident description

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