ASN Wikibase Occurrence # 284467
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Date: | Wednesday 8 August 2007 |
Time: | 18:40 LT |
Type: | Cessna T337G |
Owner/operator: | Private |
Registration: | N969CB |
MSN: | P3370222 |
Total airframe hrs: | 2484 hours |
Engine model: | Teledyne Continental TSIO-360-CB |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chamblee, Georgia -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Atlanta-DeKalb Peachtree Airport, GA (PDK/KPDK) |
Destination airport: | Akron/Canton Regional Airport, OH (CAK/KCAK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Shortly after takeoff on a hot day, after the airplane was about 10 miles from the departure airport, the rear engine failed for undetermined reasons. The pilot turned the airplane back toward the airport, feathered the rear engine, and maintained front engine power at the top of the green arc of the manifold pressure gage, at 33 inches of manifold pressure. The airplane did not maintain altitude at that power setting, and to avoid houses and vehicles on the ground, the pilot performed a forced landing at a water treatment plant. During the landing, the airplane struck the top of a concrete structure, hit the ground, and became engulfed in flames. According to the owner's manual, after an engine failure, the remaining engine power to be used isto be "increased as required." The published maximum power setting was 37 inches of manifold pressure at "red line," without any time limitations. A performance calculation indicated that at the existing ambient temperatures, and at that power setting, the airplane should have climbed at least 290 feet per minute. Additional references to the use of a 37-inch power setting, including performance calculations, were noted in the owner's manual.
Probable Cause: The pilot's failure to utilize all of the power available following an engine failure. Contributing to the accident were the failure of the rear engine for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07LA187 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB NYC07LA187
Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 17:08 |
ASN Update Bot |
Added |
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