Accident Mooney M20E N9614V,
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ASN Wikibase Occurrence # 287945
 
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Date:Sunday 31 October 2010
Time:23:30 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20E
Owner/operator:Randy Donnarumma
Registration: N9614V
MSN: 21-0020
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Seligman, Arizona -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Kingman, AZ
Destination airport:Boulder City, NV
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that shortly after takeoff, he turned to his intended heading and climbed to a predetermined cruise altitude to maintain clearance from terrain during the night visual flight rules cross-country flight. Following an uneventful cruise phase of the flight, the pilot observed what he believed to be his destination airport and initiated a descent. The pilot stated that he was unable to turn on the airport runway lights and decided to continue the descent to the airport's traffic pattern altitude of 4,500 feet mean sea level (msl) while circling the airport. During the second circle and descent, the pilot aborted the descent and began to initiate a climb whereupon the airplane impacted terrain at an elevation of about 5,200 feet msl. The pilot reported that he was surprised when local law enforcement informed him that he was in Seligman, Arizona, instead of his intended destination of Boulder City, Nevada. The pilot reported that there were no pre-impact anomalies with the airplane that would have contributed to the accident and that "all systems were working." The pilot added that prior to the flight; he estimated an approximate heading and altitude needed for the flight to his destination airport.

Probable Cause: The pilot's failure to maintain clearance from terrain while maneuvering. Contributing to the accident was the pilot's inadequate preflight and in-flight planning.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11CA036
Status: Investigation completed
Duration: 1 month
Download report: Final report

Sources:

NTSB WPR11CA036

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 17:00 ASN Update Bot Added

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