| Date: | Monday 22 February 2010 |
| Time: | 14:15 LT |
| Type: | Van's RV-7 |
| Owner/operator: | Private |
| Registration: | N209MT |
| MSN: | 71202 |
| Engine model: | Lycoming IO-360-A1A |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Oregon City, Oregon -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Hubbard, OR (7S9) |
| Destination airport: | Oregon City, OR (OG30) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he was landing at a 1,800-foot-long grass airstrip. The pilot flared the airplane approximately one-fourth of the way down the runway, the airplane bounced, and he added power to soften the second touchdown. The pilot felt that a go-around was too dangerous so he applied the brakes. Just as the airplane came to a stop, it slid into a ditch at the end of the runway. The pilot and a friend built the airplane and he had flown about 10 hours in it. He stated that he should have been more familiar with the short-field landing characteristics of this particular airplane. He had been into the airstrip numerous times in his other airplane of the same make/model, but the previous airplane was equipped with a constant speed propeller and seemed to float less down the runway.
Probable Cause: The pilot's failure to attain a proper touchdown point.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | WPR10CA145 |
| Status: | Investigation completed |
| Duration: | 3 months |
| Download report: | Final report
|
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Sources:
NTSB WPR10CA145
Location
Revision history:
| Date/time | Contributor | Updates |
| 05-Oct-2022 01:25 |
ASN Update Bot |
Added |
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