ASN Wikibase Occurrence # 290330
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Date: | Monday 29 September 2014 |
Time: | 15:10 LT |
Type: | Preiss Vans RV-9A |
Owner/operator: | Private |
Registration: | N259H |
MSN: | 90466 |
Year of manufacture: | 2002 |
Total airframe hrs: | 264 hours |
Engine model: | Lycoming O-320-E2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hobart, Oklahoma -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Grove Municipal Airport, OK (KGMJ) |
Destination airport: | Hobart Regional Airport, OK (KHBR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during his preflight calculations, he estimated that sufficient fuel was onboard the airplane to fly it to his intended destination with a 30-minute reserve. About 10 minutes from the destination airport, the fuel in the left tank was depleted, so the pilot switched to the right tank; the fuel monitor indicated that 5 gallons of fuel were remaining in the right tank. The pilot reported that, with an estimated fuel consumption rate of 6 gallons per hour, he was confident that he would reach the destination airport with fuel to spare. About 5 minutes from the airport, the fuel monitor indicated that 3 gallons of fuel were remaining in the right tank. Shortly thereafter and 2 miles east of the destination, the engine lost power. The pilot made a forced landing in a field and allowed the airplane to land hard to avoid an incipient stall. After the accident, the pilot reported that the airplane had run out of fuel. Examination of the airplane revealed that the fuel tanks were empty.
Probable Cause: A loss of engine power due to fuel exhaustion, which resulted from the pilot's erroneous preflight fuel calculations and inadequate in-flight fuel management.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA526 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB CEN14LA526
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 13:43 |
ASN Update Bot |
Added |
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