| Date: | Friday 19 June 2015 |
| Time: | 11:08 LT |
| Type: | Beechcraft 95-B55 Baron |
| Owner/operator: | |
| Registration: | N216RW |
| MSN: | TC-1956 |
| Year of manufacture: | 1976 |
| Total airframe hrs: | 3299 hours |
| Engine model: | Continental IO-470-L |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Clearwater, Florida -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Panama City-Northwest Florida Beaches International Airport, FL (ECP/KECP) |
| Destination airport: | St. Petersburg-Clearwater International Airport, FL (PIE/KPIE) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, after receiving clearance to land, he completed the before landing checklist. He added that, during the touchdown, the landing gear collapsed. According to photographs provided by the airport authority, the airplane came to rest on its belly with the right main and nose landing gears collapsed and the left main landing gear partially extended.
Postaccident examination of the landing gear system revealed that the outer sidewall of each main landing gear tire exhibited scuff marks and that the main landing gear door was scraped. Further examination revealed that both of the main landing gear extension rods were bent at the assembly actuator and that the nose landing gear extension/retraction rod was fractured. This evidence is consistent with a landing attempt with the landing gear in transit rather than fully extended as reported by the pilot. No preimpact mechanical abnormalities were noted with the landing gear system that would have precluded normal operation.
The recorded weather at the time of the accident indicated that thunderstorms existed near the airport, and photographs taken shortly after the accident show thunderstorms at the airport. Therefore, it is possible that the pilot was distracted by the approaching thunderstorm, which led to his completing the before landing checklist too late during the approach for the landing gear to fully extend before landing.
Probable Cause: The pilot's delayed completion of the before landing checklist, including the extension of the landing gear, during an approaching thunderstorm, which resulted in a landing with the landing gear in transit and the subsequent collapse of the landing gear.
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | ERA15LA249 |
| Status: | Investigation completed |
| Duration: | 5 months |
| Download report: | Final report
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Sources:
NTSB ERA15LA249
Location
Revision history:
| Date/time | Contributor | Updates |
| 07-Oct-2022 08:11 |
ASN Update Bot |
Added |
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