Accident Mooney M20J N201U,
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ASN Wikibase Occurrence # 293546
 
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Date:Sunday 26 June 2005
Time:12:54 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20J
Owner/operator:Private
Registration: N201U
MSN: 24-3156
Total airframe hrs:2818 hours
Engine model:Lycoming IO-360-A3B60
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Hailey, Idaho -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Redmond-Roberts Field, OR (RDM/KRDM)
Destination airport:Hailey-Sun Valley Airport, ID (SUN/KSUN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that he had been cleared to land. He said that he was at approximately 300 feet above ground level (AGL) when the nose of his airplane pitched up approximately 15 degrees and the left wing dropped approximately 30 degrees. He said he "attempted to correct this condition with both the ailerons and rudder, with no results. It was as if the yoke was locked with a gust lock." The pilot said that he immediately checked the location of a flight bag and oxygen bottle that were on the floor in front of the front passenger 's seat to make certain that they were not interfering with the yoke or rudders, which they weren't. He said that he had been hand flying the airplane for several minutes, but he confirmed that the auto pilot was off. The pilot said that he believed that he was approaching a stall, so he increased power to full power. Soon, thereafter, he impacted the ground after approximately 160 degrees of left hand turn. A witness said that the airplane was on a 1/4 mile final with landing gear and flaps down. He said that it looked like the airplane started to go-around to the left with a high power setting. He said that when the airplane had turned approximately 180 degrees, its left wing impacted terrain and the airplane cartwheeled. Another witness said that the airplane was never more that 100 to 150 feet above the ground during this maneuver. The pilot had recently completed (June 5, 2005) a Mooney Pilot Proficiency Program, and received his FAA required flight review endorsement. He had flown the airplane approximately 31 hours during the previous 30 days. The density altitude at the time of the accident was calculated to be 7,292 feet.

Probable Cause: The pilot's failure to maintain aircraft control while on final approach for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA05LA129
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB SEA05LA129

Revision history:

Date/timeContributorUpdates
10-Oct-2022 07:31 ASN Update Bot Added

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