ASN Wikibase Occurrence # 296234
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Date: | Saturday 1 February 2003 |
Time: | 13:00 LT |
Type: | Zenair CH 601 HDS |
Owner/operator: | Private |
Registration: | N474BG |
MSN: | 63628 |
Total airframe hrs: | 28 hours |
Engine model: | Subaru EA81 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Grandfield, Oklahoma -
United States of America
|
Phase: | Unknown |
Nature: | Test |
Departure airport: | Chattanooga, OK (92F) |
Destination airport: | Chattanooga, OK (92F) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a test flight on the morning of the accident, the engine was running rough; however, the pilot landed the airplane without further incident. The pilot removed the carburetor screen, cleaned the debris from the screen, and reinstalled the screen. During the accident flight, the oil and water temperature indicated 205-210 degrees, and the flight was returning to the airport. At an airspeed of 70 knots and an altitude of 500 feet agl, there was a total loss of engine power. The pilot performed the emergency landing procedures; however, he was not able to turn the airplane into the wind due to an unsafe landing area east of the airport traffic pattern for the runway. The pilot landed the airplane with a right quartering tailwind (25 knots, gusts 30 knots) in a field. During the landing roll, the nose landing gear struck a berm, the nose landing gear collapsed, and the airplane structure twisted as the airplane came to rest. The reason for the loss of engine power was not determined. The pilot reported the winds were from the southwest at 25 knots with gust to 30 knots. The airplane had accumulated 27.6 hours of the required 40 hours of flight time under the operating limitations for the homebuilt airplane.
Probable Cause: The loss of engine power for an undetermined reason. Contributing factors were the lack of suitable terrain for the forced landing and the unfavorable wind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA091 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB FTW03LA091
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 18:10 |
ASN Update Bot |
Added |
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