ASN Wikibase Occurrence # 297111
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 20 June 2002 |
Time: | 05:50 LT |
Type: | Beechcraft V35A Bonanza |
Owner/operator: | Private |
Registration: | N8327N |
MSN: | D8734 |
Total airframe hrs: | 3325 hours |
Engine model: | Continental IO-520-BA |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Cottonwood, AZ -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Cottonwood, AZ (P52) |
Destination airport: | Litchfield Park Airport, AZ (KGEU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During initial takeoff climb, the pilot heard a "loud bang" from the engine, followed by a smell of fuel in the cockpit, a loss of fuel pressure, and a substantial engine vibration. During an attempt to return to the airport, the engine lost power, and the pilot initiated a forced landing. During the landing, the airplane impacted a cattle gate and came to rest on its nose. Examination of the engine revealed that the #1 lower connecting rod bolt was fractured at the bolt's dowel section, which corresponded with the connecting rod and rod cap split line. According to the engine manufacturer's metallurgist, the fracture initiated at the outer diameter of the bolt's dowel section, and the fracture progressed in fatigue until the bolt fractured as a result overstress. The bolt's dowel section exhibited fretting damage at the fracture origin. At the time of the accident, the engine had accumulated 9.64 hours since the annual inspection, and 195.84 hours since major overhaul.
Probable Cause: The loss of engine power as a result of the failure of the #1 lower connecting rod bolt due to fatigue.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX02LA204 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX02LA204
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 14:33 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation