ASN Wikibase Occurrence # 30043
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Date: | Wednesday 30 August 2000 |
Time: | 09:54 |
Type: | Beechcraft E55 Baron |
Owner/operator: | Private |
Registration: | N9047V |
MSN: | TE-938 |
Total airframe hrs: | 5810 hours |
Engine model: | Teledyne Continental IO-520-C-7B |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Mississippi River, near Grafton, Illinois -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | St. Charles, MO (SET) |
Destination airport: | Zanesville, OH (ZZV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During climb after takeoff the pilot became disorientated, lost aircraft control, and the airplane impacted the Mississippi River. The instrument rated pilot departed into known instrument meteorological conditions without an instrument flight rules (IFR) air traffic control (ATC) clearance. After takeoff the pilot contacted ATC to obtain an IFR clearance to his intended destination. The ATC controller instructed the pilot to make a right turn to avoid opposite direction traffic. The traffic was on an instrument approach to the airport from which the accident airplane had just departed. During the turn the accident airplane impacted the Mississippi River approximately 2.2 nm north-northeast of the departure airport. Instrument meteorological conditions prevailed at the time of the accident with a visibility of 1-1/2 statute miles and an overcast ceiling of 300 feet above ground level. No anomalies were found with the recovered portions of the airplane that could be associated with a pre-impact condition.
Probable Cause: The pilot not maintaining aircraft control and altitude/clearance from the river. Factors to the accident included the pilot not obtaining an air traffic control clearance prior to departure into instrument meteorological conditions, the pilot becoming spatially disoriented, the low ceiling, and the mist.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI00FA276 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X21661&key=1 FAA register: 2.
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?nNumberTxt=9047V Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
01-Jun-2014 02:11 |
Dr. John Smith |
Updated [Time, Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 19:02 |
ASN Update Bot |
Updated [Total fatalities, Total occupants, Departure airport, Destination airport, Source, Narrative] |
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