| Date: | Sunday 27 November 2022 |
| Time: | 15:45 LT |
| Type: | Cessna 177A Cardinal |
| Owner/operator: | |
| Registration: | N2994X |
| MSN: | 17700394 |
| Year of manufacture: | 1967 |
| Total airframe hrs: | 3823 hours |
| Engine model: | Lycoming O-360-A4M |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Willow Spring, AZ -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Lake Havasu City Airport, AZ (KHII) |
| Destination airport: | Sedona Airport, AZ (SDX/KSEZ) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on a cross-country flight and had climbed to his en route cruising altitude. The airplane continued at that altitude for about 10 minutes and then the engine sustained a total loss of power. The pilot attempted to troubleshoot the loss of power while preparing for an off-airport landing. He estimated the airplane had about 23 gallons of fuel at this time. The pilot intentionally pulled back on the controls to deplete airspeed and avoid contacting a boulder during the forced landing. The airplane stalled, impacted the terrain, and came to rest inverted in a field.
Postaccident examination revealed no evidence of leakage in the fuel system, but only trace amounts of fuel were found throughout the system and the 23 gallons could not be accounted for. It is unknown if the fuel egressed from the system after impact. The throttle cable was attached to the carburetor arm but was damaged and could only move slightly when manipulating the control knob in the cockpit (full travel was not possible). However, the pilot reported manipulating the throttle following the power loss; therefore, the throttle cable damage most likely occurred as a result of the impact.
The air intake tubing was partially crushed and evidence was found of it having been modified. It is unknown if a lack of air to the carburetor contributed to the accident.
Probable Cause: The airplane's loss of engine power for undetermined reasons.
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | WPR23LA060 |
| Status: | Investigation completed |
| Duration: | 1 year and 6 months |
| Download report: | Final report
|
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Sources:
NTSB WPR23LA060
FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=2994X https://flightaware.com/live/flight/N2994X Location
Images:

3:42PM Local Time
Requested by Center to spot the crash site
Revision history:
| Date/time | Contributor | Updates |
| 01-Jul-2024 08:49 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, Accident report, ] |
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