Wirestrike Accident Hiller UH-12E N5388V,
ASN logo
ASN Wikibase Occurrence # 30361
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 2 November 1999
Time:12:18 LT
Type:Silhouette image of generic UH12 model; specific model in this crash may look slightly different    
Hiller UH-12E
Owner/operator:James R. Pope
Registration: N5388V
MSN: 2099
Total airframe hrs:22137 hours
Engine model:Lycoming VO-540-C2A
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Clearwater River, Nez Perce Indian Reservation, near Stites, Idaho -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Clarkston, WA
Destination airport:Grangeville, ID
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During a low-altitude fish survey, the helicopter experienced a separation of a control rotor while leveling off from a climb to about 400 feet above ground level (AGL). The pilot initiated an emergency descent but, due to severely reduced cyclic controllability resulting from the separation, was unable to avoid power lines in the aircraft's emergency descent flight path. The helicopter struck the power lines about 50 feet AGL and fell to the ground, landing hard but upright. Post-accident examination disclosed a fatigue failure in the cuff which retains the control rotor blade. The fatigue originated on two opposite sides of a retaining bolt hole that appeared to have been unevenly hand chamfered or deburred during original manufacture of the cuff, with gouging and sharp-bottomed dents visible at the origins. However, while a company mechanic had signed off an Airworthiness Directive (AD) requiring recurring inspection of the cuff about two months/56 flight hours before the accident, post-accident examination disclosed evidence indicative of inadequate inspection and maintenance of the assembly, including: old dried grease between the cuff and control rotor blade spar, large areas of the spar missing required paint with associated corrosion areas, and zinc chromate primer in corrosion pits. The FAA-approved Hiller service bulletin referenced by the AD contains procedures for inspection of spar tube retention bolt holes for 'elongation, corrosion, burrs, pitting or fretting' and associated repair procedures, but does not contain any instructions to inspect or repair bolt holes in the control rotor cuff for those same conditions.

Probable Cause: Inadequate inspection of the control rotor cuff by a company mechanic and subsequent fatigue fracture of the cuff, resulting in an inflight separation of the control rotor blade. Factors contributing to the accident were: inadequate quality control during manufacture; insufficiently defined manufacturer's inspection and repair procedures; inadequate FAA approval of the manufacturer's inspection and repair procedures; power lines in the helicopter's emergency descent flight path; and reduced aircraft controllability following the control rotor separation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA00TA013
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB SEA00TA013
FAA register: NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X20183&key=1
FAA register: 2. FAA: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=5388V

Location

Revision history:

Date/timeContributorUpdates
27-Sep-2008 01:00 ASN archive Added
13-Jun-2014 19:50 Dr. John Smith Updated [Time, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
14-Dec-2017 09:48 ASN Update Bot Updated [Time, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
07-Apr-2024 17:10 ASN Update Bot Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org