Accident Mooney M20C Mark 21 N5587Q, Saturday 28 January 2023
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Date:Saturday 28 January 2023
Time:13:10
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C Mark 21
Owner/operator:Private
Registration: N5587Q
MSN: 2982
Year of manufacture:1965
Total airframe hrs:5175 hours
Fatalities:Fatalities: 0 / Occupants: 2
Other fatalities:0
Aircraft damage: Destroyed
Category:Accident
Location:Tom B. David Field (KCZL), Calhoun, GA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Calhoun-Tom B. David Field, GA (KCZL)
Destination airport:Calhoun-Tom B. David Field, GA (KCZL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On January 28, 2023, about 1310 eastern standard time, a Mooney M20C, N5587Q, was destroyed when it was involved in an accident in Calhoun, Georgia. The pilot was seriously injured, and the flight instructor-rated passenger received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that the right magneto dropped 150 rpm when he and the flight instructor performed the engine runup. They leaned the fuel mixture and ran the engine up to about 1,700 rpm a couple of times until both magnetos dropped 125 rpm during the magneto checks. Once the magneto checks were normal, they initiated the takeoff. The pilot retracted the landing gear and a few moments later, while they were about 70 ft above the runway, there was a popping noise, the engine rpm went to nearly zero, and they began to lose altitude. They lowered the landing gear and touched down near the end of the runway. The airplane skidded off the end of the runway into the grass and slid into an earth embankment. The airplane then became airborne, rotated 90º to the left, and came to rest after a few hundred feet. The flight instructor then advised the pilot of flames near the pilot’s feet and they both exited the airplane. The airplane was destroyed by the postimpact fire.

Examination of the engine revealed that the No. 3 bottom spark plug was not in the spark plug hole and was hanging from the ignition cable. The spark plug hole thread insert (Helicoil) was partially pulled from the spark plug hole. Examination of the spark plug revealed the lower three threads of the spark plug displayed absence of rust, but the threads located above them were rusty, and the bottom portion of the Helicoil was still intact. No other anomalies were discovered with the engine that would have precluded normal operation.

Review of maintenance records indicated the engine had last been overhauled about 30 years ago, but this most probably did not contribute to the accident. The most recent annual inspection was completed about 2 months before the accident. Review of the logbook entry for the annual inspection indicated that during the annual, the spark plugs had been “removed, cleaned, inspected and installed.” The engine time in service between the last annual inspection and the last recorded entry in the engine logbook, which stated that the No. 2 cylinder spark plug was replaced was 1 hour. The investigation was not able to determine if the No. 3 cylinder spark plug was removed and reinstalled at that time. The accident occurred 14 days later.

Therefore, it is likely that the No. 3 bottom spark plug was either not inserted all the way or it wasn’t properly torqued when it was installed during the annual inspection or most recent maintenance work.

Probable Cause: A partial loss of engine power during the initial climb due to an improperly installed spark plug.

Accident investigation:
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Investigating agency: NTSB
Report number: ERA23LA120
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

https://www.atlantanewsfirst.com/2023/01/28/calhoun-police-pilot-passenger-escape-crash-before-plane-catches-fire/
https://www.fox5atlanta.com/news/calhoun-airport-plane-crash-fire

https://data.ntsb.gov/Docket?ProjectID=106649
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?NNumberTxt=5587Q

History of this aircraft

Other occurrences involving this aircraft

10 March 1983 N5587Q Private 0 Solon Springs, WI sub

Location

Images:


Photo: NTSB

Media:

Revision history:

Date/timeContributorUpdates
22-Feb-2025 04:30 Captain Adam Updated [Phase, Source, Narrative, Accident report, Photo, ]

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