ASN Wikibase Occurrence # 30783
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Date: | Friday 9 April 1999 |
Time: | 20:15 |
Type: | Bell 206L-4 LongRanger IV |
Owner/operator: | Minnesota State Patrol |
Registration: | N119SP |
MSN: | 3151 |
Year of manufacture: | 1980 |
Total airframe hrs: | 6703 hours |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Cloquet, Cartlton County, Minnesota -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Minneapolis, MN (MIC) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he was 10 miles from Cloquet Carlton County Airport when he noticed a low fuel pressure warning. The pilot stated that he knew of a field that he could land in, five miles from his current position, and decided to maneuver the helicopter to that location. The pilot reported that while over the predetermined field, at approximately 300 feet above ground level, the engine lost total power and he began an autorotation towards the field. The pilot stated that he performed a run-on landing, in order to avoid two posts, and came to rest in an upright attitude. The pilot reported that he did not see the reflecting posts until the aircraft was near the ground because of the low light condition. The pilot reported that he had 35-gallons of fuel when he departed Crystal Airport at 1905. The pilot stated that the flight time, from Crystal Airport to Cloquet Carlton County Airport, was typically 1.2 hours to 1.5 hours. According to the Chief Pilot of the Minneapolis State Police, the fuel burn for the accident helicopter was 25 gallons/hour. In a telephone conversation with the investigator-in-charge, the pilot indicated that he ran out of fuel during the accident flight.
Probable Cause: The pilot's inadequate fuel management which led to fuel exhaustion and subsequent loss of engine power. Related factors were the pole and dusk light conditions.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001205X00439&key=1 FAA register: 1. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=119SP Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
10-Apr-2015 18:00 |
Dr. John Smith |
Updated [Date, Time, Aircraft type, Registration, Cn, Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
26-Nov-2017 12:43 |
ASN Update Bot |
Updated [Time, Cn, Operator, Departure airport, Destination airport, Source, Narrative] |
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