Accident Cessna 402C C6-KEV,
ASN logo
ASN Wikibase Occurrence # 314039
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Friday 21 April 2006
Time:
Type:Silhouette image of generic C402 model; specific model in this crash may look slightly different    
Cessna 402C
Owner/operator:Cambridge Air Services
Registration: C6-KEV
MSN: 402-0051
Year of manufacture:1967
Fatalities:Fatalities: 0 / Occupants:
Aircraft damage: Substantial
Category:Accident
Location:Freeport-Grand Bahama International Airport (FPO/MYGF) -   Bahamas
Phase: Landing
Nature:Unknown
Departure airport:Fort Lauderdale-Executive Airport, FL (FXE/KFXE)
Destination airport:Freeport-Grand Bahama International Airport (FPO/MYGF)
Investigating agency: DCABah
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that approximately 20 miles out of Freeport, both hydraulic pressure lights illuminated on the annunciator panel. He extended the gear and noticed only the right gear safe light illuminated. The pilot obtained the assistance of a passenger, who retrieved the aircraft pilot operating hand book and read the appropriate procedures as the pilot followed the instructions for emergency gear extension.
The pilot stated that he landed the aircraft on the right main gear, hoping this action would release th
left main and nose gear.
After realizing that this manoeuvre was not successful, he decided to initiate a go-around. Before he could get the aircraft airborne the left propeller made contact with the ground.
The aircraft touched down approximately 9,000 feet from the threshold of runway 06; which has a total length of 11,000 feet. The aircraft travelled approximately 1,500 feet on its right main wheel before it veered off the left shoulder of the runway, struck several trees and finally came to rest pointing in a north westerly direction. The approximate final position was measured to be 180 feet from the side of the runway. The aircraft left wing burst into flames. The left wing and left side of the fuselage was substantially damaged by fire. The four occupants escaped with only minor injuries.


Probable Cause
The investigation determines that the probable causes of this accident to be the following;
• Substandard maintenance that was performed. (Due to the improper flange on the hydraulic line, the hydraulic line came loose from its housing and depleted the fluid from the hydraulic reservoir).
• Failure of the back up emergency blow down bottle system. It has been determined from inspection that the cable that connects the emergency blow down bottle system in the nose well of the aircraft to the T-handle in the cockpit, exhibited excessive play. Therefore even though the cable was pulled all the way to its fullest extent, it did not allow movement of the pin that would have provided activation of the system. Annual inspection report completed in December 2005 revealed that the portion of the Annual Inspection that required inspection of the emergency blow down bottle was not signed off by the mechanic as having been accomplished. However, the aircraft was returned to service with this discrepancy outstanding.
• Pilot’s lack of qualification and unfamiliarity with this aircraft, its systems and emergency procedures. ( Evidence of falsification of qualification and time requirement exists in pilot’s logbook)
• Pilot’s poor decision making and impaired judgement. (Possibility of impaired judgement due to pilot fatigue).
• Pilot’s failure in assessing the severity of his situation.
• Pilot’s failure to notify ATC of his problem. (Problem was discovered 20 miles prior to the accident).
• Pilot’s failure to properly assess the conditions for landing and maintain vigilant situational awareness while manoeuvring the aircraft after landing. (From post accident inspection, it was noted that the flaps were not extended for the landing. Had it been extended the aircraft glide path as well as the distance required for roll out after landing may have been greatly decreased).
• Pilot’s failure to take immediate action once he realized his predicament. (Pilot stated that after the propeller made contact with the ground, he decided to apply power and go around, but it was too late. Failure to act also can be attributed to possible pilot fatigue as (pilot was out all day shopping and then decided to leave at such a late hour) well as pilot’s unfamiliarity with aircraft systems and performance capabilities).
• Pilot’s failure to request Emergency Service Assistance. Had this service been requested in a timely manner, preparations could have been made to prevent the fire from spreading to the degree in which it did.

Accident investigation:
cover
  
Investigating agency: DCABah
Report number: 
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

DCA

Revision history:

Date/timeContributorUpdates
30-May-2023 20:42 harro Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org