| Date: | Saturday 11 February 2023 |
| Time: | 13:50 LT |
| Type: | Learjet 55 |
| Owner/operator: | 1982-047 LLC |
| Registration: | N600C |
| MSN: | 55-047 |
| Year of manufacture: | 1982 |
| Total airframe hrs: | 10504 hours |
| Engine model: | Honeywell TFE-731 |
| Fatalities: | Fatalities: 0 / Occupants: 6 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Rochester-Greater Rochester International Airport, NY (ROC/KROC) -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Palm Beach Airport, FL (PBI/KPBI) |
| Destination airport: | Rochester-Greater Rochester International Airport, NY (ROC) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Learjet 55, N600C, was substantially damaged when it made a hard landing at Rochester-Greater Rochester International Airport, NY (ROC).
Neither pilot reported identifying any mechanical issues with the airplane before the flight. The flight was uneventful and both pilots described the landing as being firm, with the copilot stating the landing was in the touchdown zone on the runway. The pilot reported that after landing he knew something was wrong because the left wing was low. The pilots taxied the airplane to the ramp where they discovered fuel leaking from the left wing.
A review of airport surveillance video revealed that the airplane touched down around the displaced threshold, bounced, and touched down again. Examination of the runway revealed skid marks beginning in the displaced threshold about 110 ft before the landing surface of the runway. Fractured airplane parts were scattered over and beyond the ground scars and tire markings. Postaccident examination of the airplane revealed it sustained structural and skin damage to the left wing, the landing gear strut, and both left main wheels.
One passenger said that she heard altitudes called out during the landing approach, and just before touchdown, she heard a crewmember announce, “too fast, too fast!' She stated the airplane contacted the runway so hard the oxygen masks deployed and compartments inside the airplane opened. The airplane bounced, and the second landing was bumpy. She also stated that fuel was leaking from the airplane when they were deplaned.
Although the pilots' subsequent statements indicated that they observed that the airplane's left wing was “lower' during takeoff on the accident flight, surveillance video of the airplane from the departure airport did not indicate any anomalies. Given the available evidence, it is likely that the pilots failed to attain a proper landing flare and touchdown point, which resulted in a hard landing short of the runway.
Probable Cause: The pilots' failure to attain a proper landing flare and touchdown point, which resulted in a hard landing short of the runway.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | ERA23LA126 |
| Status: | Investigation completed |
| Duration: | 1 year and 7 months |
| Download report: | Final report
|
|
Sources:
NTSB ERA23LA126
Location
Revision history:
| Date/time | Contributor | Updates |
| 27-Oct-2024 20:48 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, ] |
| 27-Oct-2024 20:58 |
ASN |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Narrative, ] |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation