Loss of control Accident Learjet 35A N880Z, Monday 27 December 2021
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Date:Monday 27 December 2021
Time:20:14 LT
Type:Silhouette image of generic LJ35 model; specific model in this crash may look slightly different    
Learjet 35A
Owner/operator:Aeromedevac Air Ambulance
Registration: N880Z
MSN: 591
Year of manufacture:1985
Total airframe hrs:13582 hours
Engine model:Honeywell TFE731-2-2B
Fatalities:Fatalities: 4 / Occupants: 4
Other fatalities:0
Aircraft damage: Destroyed, written off
Category:Accident
Location:El Cajon, San Diego -   United States of America
Phase: Approach
Nature:Ferry/positioning
Departure airport:Santa Ana-John Wayne International Airport, CA (SNA/KSNA)
Destination airport:El Cajon, CA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
A Learjet 35A crashed in a residential area, killing all on board. The aircraft was completing the turn for the final approach to runway 27R at San Diego-Gillespie Field, California. It struck Pepper Drive in a residential area of El Cajon, San Diego, 2,6 km east of the runway threshold and burst into flames.

Earlier on the day of the accident, the flight crew had conducted a patient transfer from a remote airport to another nearby airport. Following the patient transfer, the flight crew departed under night conditions to return to their home base.

Review of air traffic control (ATC) communication, as well as cockpit voice recorder (CVR) recordings, showed that the flight crew initially was cleared on the RNAV (GPS) runway 17 instrument approach. The approach plate for the instrument approach stated that circling to runway 27R and 35 was not authorized at night.

Following the approach clearance, the flight crew discussed their intent to cancel the approach and circle to land on runway 27R. Additionally, the flight crew discussed with each other if they could see the runway. Once the flight crew established visual contact with the runway, they requested to squawk VFR, then the controller cleared them to land on runway 17. The flight crew then requested to land on runway 27. The controller asked the pilot if they wanted to cancel their instrument flight rules (IFR) flight plan, to which the pilot replied, “yes sir.' The controller acknowledged that the IFR cancellation was received and instructed the pilot to overfly the field and enter left traffic for runway 27R and cleared them to land.

Shortly after, the flight crew asked the controller if the runway lights for runway 27R could be increased; however, the controller informed them that the lights were already at 100 percent. Just before the controller's response, the copilot, who was the pilot flying, then asked the captain “where is the runway.' As the flight crew maneuvered to a downwind leg, the captain told the copilot not to go any lower; the copilot requested that the captain tell him when to turn left. The captain told him to turn left about 10 seconds later. The copilot stated, “I see that little mountain, okay' followed by both the captain and co-pilot saying, “woah woah woah, speed, speed' 3 seconds later. During the following 5 seconds, the captain and copilot both stated, “go around the mountain' followed by the captain saying, “this is dicey' and the co-pilot responding, “yeah it's very dicey.' Shortly after, the captain told the copilot “here let me take it on this turn' followed by the co-pilot saying, “yes, you fly.' The captain asked the copilot to watch his speed, and the copilot agreed. About 1 second later, the copilot stated, “speed speed speed, more more, more more, faster, faster… .' Soon after, the CVR indicated that the airplane impacted the terrain.

Automatic dependent surveillance – broadcast (ADS-B) data showed that at the time the flight crew reported the runway in sight, they were about 360 ft below the instrument approach minimum descent altitude (MDA), and upon crossing the published missed approach point they were 660 ft below the MDA. The data showed that the flight overflew the destination airport at an altitude of about 775 ft mean sea level (msl), or 407 ft above ground level (agl), and entered a left downwind for runway 27R. While on the downwind leg, the airplane descended to an altitude of 700 ft msl, then ascended to an altitude of 950 ft msl while on the base leg. The last recorded ADS-B target was at an altitude of 875 ft msl, or about 295 ft agl.

Examination of the accident site revealed that all major structural components of the airplane were present within the wreckage debris path. Wreckage and impact signatures were consistent with a nose-low impact with terrain. Postaccident examination of the engine revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation.

Information provided during interviews with the controller in charge (CIC), revealed that he was aware that the weather had been marginal visual flight rules (MVFR) for a while leading up to the time of the accident. He recalled the weather at the time of the accident as still being MVFR and did not recall it ever becoming IFR, and further stated he had not observed a change on the automated weather observing system (AWOS) display, which was located in the back of the tower cab and did not have an audible alert when weather conditions changed. At the time of the accident, the CIC was operating in a position responsible for conducting Limited Aviation Weather Reporting Station (LAWRS) augmentation.

According to information provided during interviews with the local control (LC) controller, he was aware that the weather had been marginal most of his shift. He recalled the weather at the time of the accident as still being MVFR and did not recall it ever becoming IFR. At the time of the event, he was not directly responsible for conducting LAWRS augmentation.

The AWOS one-minute data showed that the visibility had decreased to less than 3 miles visibility 7 minutes before the flight crew had checked in with tower controller on the instrument approach. The visibility remained below 3 miles throughout the instrument approach, cancelation of the IFR clearance, and accident sequence.

A performance study was conducted to determine the estimated airspeed, bank angle, and angle-of-attack. The study indicated that the flight crew likely exceeded the wings' critical angle-of-attack, and the airplane entered an accelerated aerodynamic stall at a low altitude that would have not allowed time for recovery.

Probable Cause: The flight crew's decision to descend below the published MDA, cancel their IFR clearance to conduct an unauthorized circle-to-land approach to another runway while the airport was in nighttime IFR conditions, and the exceedance of the airplane's critical angle of attack, and subsequently entering an aerodynamic stall at a low altitude. Contributing to the accident was the tower crew's failure to monitor and augment the airport weather conditions as required, due in part to, the placement of the AWOS display in the tower cab and the lack of audible AWOS alerting.

METAR:

02:55 UTC / 18:55 local time:
KSEE 280255Z VRB05KT 3SM BR BKN020 OVC026 10/08 A2998

03:55 UTC / 19:55 local time:
KSEE 280355Z VRB05KT 3SM BR SCT011 BKN020 11/09 A2996

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR22FA068
Status: Investigation completed
Duration: 2 years and 6 months
Download report: Final report

Sources:

NTSB WPR22FA068

Location

Images:


photo (c) Flightaware; El Cajon, San Diego; 27 December 2021


Recorded ADS-B data with ATC communication annotations (NTSB)

Revision history:

Date/timeContributorUpdates
20-Jul-2024 09:19 ASN Update Bot Updated [Time, Cn, Operator, Other fatalities, Destination airport, Source, Narrative, Category, ]
20-Jul-2024 09:45 ASN Updated [Operator, Narrative, ]
20-Jul-2024 09:48 ASN Updated [Photo, ]

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