ASN Wikibase Occurrence # 32339
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Date: | Thursday 1 September 1994 |
Time: | 13:10 LT |
Type: | Sikorsky S-64F (CH-54B) |
Owner/operator: | Erickson Air Crane Company |
Registration: | N165AC |
MSN: | 64085 |
Year of manufacture: | 1969 |
Total airframe hrs: | 1724 hours |
Engine model: | P&W JFTD12-5A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hanging Flower Lake, Libby, MT -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | , MT (S59) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER WAS ON A MAINTENANCE TEST FLIGHT TO TEST A RETARDANT TANK SYSTEM THAT WAS USED TO CARRY AND DISPENSE WATER. AFTER ARRIVING AT A LAKE, THE FLIGHT CREW HOVERED THE HELICOPTER WHILE LOWERING THE SNORKEL TO ONLOAD WATER. HOWEVER, THE QUANTITY INDICATOR WAS MALFUNCTIONING, AND THE CREW MEMBERS WERE UNSURE IF WATER WAS BEING ONLOADED. THE PILOT OPTED TO FLY OUT OF THE HOVER AND DUMP THE WATER FROM THE RETARDANT TANK. AS THE FLIGHT BEGAN TO DEPART THE AREA, THE PILOT NOTED THAT THE HELICOPTER WAS LACKING RESPONSE TO THE COLLECTIVE AND THE RATE OF CLIMB WAS SLOW. WHEN THE WATER WOULD NOT DUMP FROM THE TANK, THE FLIGHT CREW TRIED TO JETTISON THE TANK. NEITHER SYSTEM WOULD WORK. THE ROTOR RPM BEGAN TO DECREASE AND THE HELICOPTER SETTLED INTO THE WATER AND SANK. DURING AN INVESTIGATION, NO MECHANICAL FAILURE OR MALFUNCTION OF EITHER ENGINE WAS FOUND. WHEN CHECKED, THE RETARDANT (WATER) QUANTITY INDICATOR SYSTEM WAS INOPERATIVE AND WOULD ONLY SENSE THAT THERE WAS NO WATER IN THE TANK. TO RELEASE WATER, THE SYSTEM NEEDED TO SENSE THAT THERE WAS ENOUGH WATER FOR THE SELECTED SETTING; THEREFORE, THE TANK DOORS WOULD NOT OPEN TO DUMP WATER WITH THIS MALFUNCTION. NO EVIDENCE WAS FOUND TO DETERMINE WHY THE EMERGENCY TANK DROP SYSTEM DID NOT FUNCTION. USING ESTIMATES, PERFORMANCE DATA INDICATED THE HELICOPTER WAS ABOVE THE MAXIMUM GROSS WEIGHT AND WAS POWER LIMITED FOR THE ENVIRONMENTAL CONDITIONS. ELEVATION OF THE LAKE WAS ABOUT 6500 FEET; AIR TEMPERATURE WAS ABOUT 63 DEGREES.
Probable Cause: THE FLIGHT CREW ALLOWED THE HELICOPTER'S WEIGHT AND BALANCE TO BE EXCEEDED, AND THE EXTERNAL LOAD (TANK) JETTISON SYSTEM FAILED TO OPERATE. A FACTOR RELATED TO THE ACCIDENT WAS: THE FALSE INDICATION ON THE RETARDANT QUANTITY INDICATOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA94LA228 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB SEA94LA228
Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
19-Mar-2011 05:28 |
TB |
Updated [Source, Narrative] |
19-Mar-2011 05:47 |
TB |
Updated [Time, Phase, Nature, Source, Narrative] |
19-Mar-2011 05:49 |
TB |
Updated [Departure airport, Source] |
19-Mar-2011 05:50 |
TB |
Updated [Source] |
09-Apr-2024 19:36 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Nature, Departure airport, Source, Narrative, Category, Accident report] |
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