| Date: | Wednesday 15 December 1993 |
| Time: | 13:05 |
| Type: | Mitsubishi Mu-300 Diamond IA |
| Owner/operator: | Whitham Farm Feedyard Inc |
| Registration: | N710MB |
| MSN: | A078SA |
| Year of manufacture: | 1984 |
| Total airframe hrs: | 2593 hours |
| Engine model: | Pratt & Whitney Canada JT15D-4 |
| Fatalities: | Fatalities: 3 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed, written off |
| Category: | Accident |
| Location: | ca 13 km SE of Goodland-Renner Field, KS (GLD) -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Scott City Municipal Airport, KS (KTQK) |
| Destination airport: | Goodland-Renner Field, KS (GLD/KGLD) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Mitsubishi MU-300 corporate jet, N710MB, impacted the terrain after being cleared for the ILS runway 30 approach at Goodland Municipal, KS. The airplane was destroyed by the impact and post- accident fire. The crew of two and the one passenger aboard received fatal injuries. The flight departed Scott City Municipal Airport, KS, at 12:48 with the intended destination of Glasgow International Airport, MT (GGW), with an intermediate stop at Goodland-Renner Field, KS (GLD).
The flight was cleared for the ILS approach to runway 30. The flying pilot was the pilot-in-command. According to the cockpit voice recorder transcripts, the flying pilot had difficulty making a stabilized approach. During the initial descent the airplane entered an over-speed condition and the airplane flew through the localizer. During his attempt to re-establish the airplane on the localizer, the pilot allowed the airspeed to decrease to the point where the prestall 'stick-shaker' activated. The stick shaker continued until the airplane departed controlled flight and impacted terrain.
PROBABLE CAUSE: "The pilot-in-command's inadvertent stall of the airplane. A factor associated with the accident is the pilot-in-command's poor IFR procedures."
Accident investigation:
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| Investigating agency: | NTSB |
| Report number: | CHI94FA050 |
| Status: | Investigation completed |
| Duration: | 10 months |
| Download report: | Final report
|
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Sources:
NTSB
Location
Revision history:
| Date/time | Contributor | Updates |
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