| Date: | Friday 1 September 2023 |
| Time: | 12:51 |
| Type: | Beechcraft B200C Super King Air |
| Owner/operator: | Tropicair |
| Registration: | P2-JAU |
| MSN: | BL-39 |
| Year of manufacture: | 1981 |
| Total airframe hrs: | 24019 hours |
| Cycles: | 23214 flights |
| Engine model: | Pratt and Whitney Canada PT6A-42 |
| Fatalities: | Fatalities: 0 / Occupants: 7 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Port Moresby-Jacksons International Airport (POM/AYPY) -
Papua New Guinea
|
| Phase: | Landing |
| Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
| Departure airport: | Tari Airport (TIZ/AYTA) |
| Destination airport: | Port Moresby-Jacksons International Airport (POM/AYPY) |
| Investigating agency: | AIC PNG |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Beechcraft B200C Super King Air suffered a nose gear collapse on landing at Port Moresby-Jacksons International Airport (POM). There were no injuries.
The crew reported that they became aware of an unsafe landing gear condition in flight and, in coordination with ground services, attempted to rectify the issue but the issue persisted. They subsequently requested for Jacksons Emergency Services to standby for their landing.
The aircraft landed on runway 14R. The crew reported that immediately after landing, the nose landing gear collapsed.
Causes [Contributing factors]
The NLG collapse during landing roll was determined to have occurred because the NLG did not fully extend and lock into the fully extended position. The investigation found that this was due to the internal failure of the NLG Actuator.
Further inspections of the faulty NLG Actuator by the manufacturer found that the actuators nut assembly threads were excessively worn, allowing the nut assembly to freely move through the screw housing without any thread engagement. The grease in the nut assembly was found to be thick and dry.
The operator had carried out the NLG Actuator lubrication at specified due intervals required by the manufacturer, however, the dry and thick grease identified in the nut assembly indicates that there may have been inadequate grease or lubricant in the nut assembly which depleted overtime, resulting in the nut assembly threads excessively wearing out before the next service (inspection and lubrication) of the NLG Actuator was due.
The NLG Actuator lubrication carried out by the operator at specified due intervals were incorrectly referenced. The NLG Actuator lubrication procedure, if correctly referenced, would have directed the maintenance personnel to a separate NLG Actuator inspection procedure which is required to be performed to determine whether the actuator should be returned to service and inspected at specified intervals, overhauled or replaced before partially disassembling the actuator for lubrication. The investigation found that there were no records of this coinciding NLG Actuator inspection procedure.
Accident investigation:
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| Investigating agency: | AIC PNG |
| Report number: | AIC 2023-1005 |
| Status: | Investigation completed |
| Duration: | 11 months |
| Download report: | Final report
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Sources:
NOTAM, PNG Media, Eye witness report
https://www.flightradar24.com/data/aircraft/p2-jau#31d61344 PNG AIC
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
| Date/time | Contributor | Updates |
| 01-Sep-2023 12:58 |
Petropavlovsk |
Added |
| 01-Sep-2023 13:52 |
gerard57 |
Updated |
| 01-Sep-2023 14:24 |
harro |
Updated |
| 03-Sep-2023 11:40 |
harro |
Updated |
| 27-Sep-2023 11:17 |
harro |
Updated |
| 22-Aug-2024 09:43 |
ASN |
Updated [Narrative, Accident report, ] |