| Date: | Monday 4 September 2023 |
| Time: | 10:31 |
| Type: | Beechcraft A36 Bonanza |
| Owner/operator: | Private |
| Registration: | N1WN |
| MSN: | E-2681 |
| Year of manufacture: | 1991 |
| Total airframe hrs: | 1935 hours |
| Engine model: | Continental IO-550 B1F |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Frankfort-Capital City Airport (FFT/KFFT), Frankfort, KY -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Gary/Chicago International Airport, IN (GYY/KGYY) |
| Destination airport: | Greenwood County Airport, SC (GRD/KGRD) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On September 4, 2023, at 1031 eastern daylight time, a Beech A36, N1WN, was substantially damaged when it was involved in an accident near Frankfort, Kentucky. The pilot and three passengers were not injured. The flight was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot and his passengers were at cruise flight when the engine stopped producing power and the propeller continued to windmill. The pilot performed a forced landing to an airport; however, when he realized that the airplane would not reach the runway he landed with the landing gear retracted on airport property, resulting in substantial damage to the airplane. The engine had accumulated fewer than 30 hours since factory overhaul.
Postaccident examination revealed that the inboard fuel vent lines were obstructed by insect nests; however, the engine ran at idle power settings during the postaccident engine test run. The engine was not tested at higher power settings due to the crankshaft being bent. Although it is possible that the obstructed fuel vents reduced fuel flow to the engine at higher power settings, the postaccident examination of the engine did not reveal evidence of preimpact malfunctions or failures that would have precluded normal operation; thus, the reason for the loss of engine power could not be determined.
Probable Cause: A total loss of engine power for reasons that could not be determined.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | ERA23LA363 |
| Status: | Investigation completed |
| Duration: | 10 months |
| Download report: | Final report
|
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Sources:
NTSB ERA23LA363
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=1WN https://data.ntsb.gov/Docket?ProjectID=193003 https://www.flightaware.com/live/flight/N1WN Location
Images:

Photo: NTSB
Revision history:
| Date/time | Contributor | Updates |
| 04-Sep-2023 17:46 |
Captain Adam |
Added |
| 04-Sep-2023 18:57 |
harro |
Updated |
| 05-Sep-2023 08:06 |
Anon. |
Updated |
| 05-Sep-2023 18:31 |
Captain Adam |
Updated |
| 06-Sep-2023 05:48 |
johnwg |
Updated |
| 06-Sep-2023 16:04 |
Captain Adam |
Updated |
| 20-Jul-2024 08:15 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, ] |
| 29-Jul-2024 15:12 |
Captain Adam |
Updated [Time, Operator, Source, Narrative, ] |
| 29-Jul-2024 15:13 |
Captain Adam |
Updated [Source, Photo, ] |
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