| Date: | Wednesday 29 January 1992 |
| Time: | 09:33 LT |
| Type: | Bellanca 17-30 Viking 300 |
| Owner/operator: | Sludge Disposal, Inc. |
| Registration: | N4869V |
| MSN: | 30115 |
| Total airframe hrs: | 1885 hours |
| Engine model: | Lycoming IO-540-D |
| Fatalities: | Fatalities: 1 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Oklahoma City, OK -
United States of America
|
| Phase: | Initial climb |
| Nature: | Executive |
| Departure airport: | |
| Destination airport: | Van Horn, TX (KVHN) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACCORDING TO THE RIGHT SEAT PILOT-IN-COMMAND, THE LEFT SEAT NON-INSTRUMENT RATED PILOT MADE THE IFR TAKEOFF. THE AIRPLANE SETTLED INTO TREES AS THE PIC WAS LOOKING AT A CHART & PUTTING A VOR INTO THE LORAN. THE PIC WAS AN EMPLOYEE OF THE LEFT SEAT PILOT. TOXICOLOGICAL TEST RESULTS ON THE LEFT SEAT PILOT REVEALED DIPHENHYDRAMINE AND PHENYLPROPANOLAMINE (ANTIHISTAMINES) IN THE URINE.
Probable Cause: THE SECOND PILOT'S (LEFT SEAT) FAILURE TO ATTAIN A POSITIVE RATE-OF-CLIMB DURING AN INSTRUMENT TAKEOFF, AND INADEQUATE SUPERVISION BY THE PILOT-IN-COMMAND. FACTORS WERE: THE WEATHER, AND THE COPILOT'S LACK OF INSTRUMENT FLIGHT TIME AND TRAINING.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | FTW92FA061 |
| Status: | Investigation completed |
| Duration: | 1 year and 11 months |
| Download report: | Final report
|
|
Sources:
NTSB FTW92FA061
Location
Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 11-Apr-2024 09:16 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report, ] |
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