| Date: | Sunday 23 May 1999 |
| Time: | 18:45 LT |
| Type: | Cessna 172RG |
| Owner/operator: | Private |
| Registration: | N9475B |
| MSN: | 172RG0834 |
| Total airframe hrs: | 3549 hours |
| Engine model: | Lycoming O-360 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Morristown, NJ -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Ocean City, MD (KOXB) |
| Destination airport: | (KMMU) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that she received her approach clearance about 12 miles from the airport. At that time, she lowered the landing gear and performed a 'gumps' check which included checking the gas, undercarriage, mixture and propeller. After lowering the landing gear, she observed a green landing gear light. The landing seemed normal, and the pilot did not hear a gear warning horn. The right main landing gear collapsed and the airplane spun 180 degrees on the runway. Examination of the wreckage by a Federal Aviation Administration Inspector, and a local mechanic, did not reveal any pre-impact mechanical malfunctions.
Probable Cause: The right main landing gear collapsed for undetermined reasons.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | NYC99LA154 |
| Status: | Investigation completed |
| Duration: | 1 year and 4 months |
| Download report: | Final report
|
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Sources:
NTSB NYC99LA154
Revision history:
| Date/time | Contributor | Updates |
| 09-Mar-2024 12:27 |
ASN Update Bot |
Added |
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