ASN Wikibase Occurrence # 35356
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Date: | Wednesday 16 September 1998 |
Time: | 07:45 |
Type: | Beechcraft 58 Baron |
Owner/operator: | State Of Wisconsin Department of Administration (DOA) |
Registration: | N4574Q |
MSN: | TH-374 |
Year of manufacture: | 1973 |
Total airframe hrs: | 7735 hours |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Oakdale, WI -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Dane County Regional Airport, WI (KKMSN) |
Destination airport: | Burnett County Airport, WI (KRZN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On September 16, 1998, at 0745 central daylight time, a Beech 58, N4574Q, operated by the State of Wisconsin's Department of Administration (DOA), impacted terrain while diverting to Volk Field (VOK), Camp Douglas, Wisconsin, after the airline transport rated pilot had declared an emergency and reported smoke in the aircraft. The aircraft was destroyed. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 business flight was operating on an instrument flight rule (IFR) flight plan. The pilot and two passengers sustained fatal injuries. The flight originated from the Dane County Regional Airport (MSN), Madison, Wisconsin, at 0653, and was en route to the Burnett County Airport (RZN), Siren, Wisconsin.
At 8,100 feet mean sea level (msl), the pilot reported smoke coming from the aircraft at 0739:32 central daylight time. At 0743:14, the aircraft altitude was 3,000 feet msl. The last received transmission by the pilot was at 0743:01. The Beech 58 Pilot's operating manual, states, under ELECTRICAL SMOKE OR FIRE, that the Battery and Alternator Switches are to be selected in the OFF position. A resistor, similar in size, shape and color to two of the resistors in the door seal inflation system was found attached to the right cabin side wall. The area surrounding the resistor revealed that a black material attached to the interior side wall was absent. There was bubbling of the black material and outside paint. Black material similar to the material on the side wall was also present on the bottom of the resistor. Installation instructions referencing the resistor, state, 'mount to metal structure for heat sink'. An emergency descent from an altitude of 8,000 feet msl was performed in a flight training simulator and a descent rate of approximately 6,200 feet per minute was obtained. A simulated off airport landing, in a simulator, was completed in approximately 02:15 minutes. Airworthiness Directive 98-21-21 has been issued for the deactivating or the removing of all provisions of the inflatable door seal installation.
Probable Cause: The installation of the door seal inflation system by company personnel. An additional cause was the emergency procedures not followed by the pilot-in-command. A contributing factor was the trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X11010 Images:
Photos: NTSB
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
13-Oct-2022 10:43 |
Captain Adam |
Updated [Operator, Departure airport, Destination airport, Narrative, Accident report, Photo] |
13-Oct-2022 10:44 |
Captain Adam |
Updated [Photo] |
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