| Date: | Saturday 22 August 1998 |
| Time: | 20:45 LT |
| Type: | Mooney M-20C |
| Owner/operator: | Private |
| Registration: | N6532U |
| MSN: | 2315 |
| Engine model: | Lycoming O-360-AID |
| Fatalities: | Fatalities: 0 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Kent Island, MD -
United States of America
|
| Phase: | Take off |
| Nature: | Private |
| Departure airport: | (3W3) |
| Destination airport: | Trenton, NJ (KTTN) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot began the takeoff roll from the sod runway 'using a soft field technique.' He applied back pressure on the yoke and then full throttle. The pilot reported the engine provided full takeoff power. Witnesses reported the airplane in a nose-high attitude as it dragged its tail the length of the runway. The airplane went off the departure end of the runway and came to rest in the Chesapeake Bay. Examination of the airplane after the accident revealed the flaps were fully retracted.
Probable Cause: the pilot's improper takeoff technique and his failure to abort the takeoff.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | IAD98LA099 |
| Status: | Investigation completed |
| Duration: | 2 years |
| Download report: | Final report
|
|
Sources:
NTSB IAD98LA099
Location
Revision history:
| Date/time | Contributor | Updates |
| 10-Mar-2024 16:39 |
ASN Update Bot |
Added |
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