Accident Beechcraft 58 Baron N721MD,
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ASN Wikibase Occurrence # 35469
 
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Date:Sunday 19 November 1995
Time:18:39 LT
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Mrd Leasing
Registration: N721MD
MSN: TH-1753
Total airframe hrs:45 hours
Engine model:Continental IO-550-C
Fatalities:Fatalities: 3 / Occupants: 5
Aircraft damage: Destroyed
Category:Accident
Location:Cleveland, OH -   United States of America
Phase: Take off
Nature:Private
Departure airport:, OH (KBKL)
Destination airport:Raleigh-durham, NC
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot received a weather briefing and filed an IFR flight plan for a night/cross-country flight. For departure from runway 24R, he was given clearance for a right turn after takeoff to a heading of 350, then he was cleared for takeoff. The tower controller stated that after the airplane was airborne, he instructed the pilot to contact departure control. The pilot acknowledged, then no further transmission was received from the plane. The controller last saw the airplane at an altitude of about 100 to 200 feet AGL, near the end of the 6,198 foot runway, when it began a right turn to a northerly heading. He then diverted his attention to other work. Subsequently, the airplane crashed on a lake north of the airport. Two passengers survived. They noted no problem with the pilot or airplane before water contact. No preimpact mechanical malfunction or failure of the airplane was found. The pilot of another airplane, who departed shortly after the accident flight, reported he was disoriented when he turned north during departure. He stated there was no visible horizon, overcast clouds blocked light from above, and there were no lights from below. Due to darkness over the lake, he had to '...stay on the instruments...until above the overcast.'

Probable Cause: the pilot's improper IFR procedure, by failing to maintain a positive rate of climb (and terrain clearance) after takeoff. Factors relating to the accident were: darkness, and the lack of visual references over water and under overcast cloud conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: BFO96FA022
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB BFO96FA022

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:22 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 10:58 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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